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British Airways Flight 38

British Airways Flight 38 was a scheduled international passenger flight from Beijing Capital International Airport in Beijing, China, to London Heathrow Airport in London, United Kingdom, an 8,100-kilometre (4,400 nmi; 5,000 mi) trip. On 17 January 2008, the Boeing 777-200ER aircraft operating the flight crashed just short of the runway while landing at Heathrow.[1][2][3] No fatalities occurred; of the 152 people on board, 47 sustained injuries, one serious.[4] It was the first time in the aircraft type's history that a Boeing 777 was declared a hull loss and subsequently written off.[5][6]

British Airways Flight 38
G-YMMM after the crash at London Heathrow Airport.
Accident
Date17 January 2008 (2008-01-17)
SummaryFuel starvation caused by ice in the fuel-oil heat exchangers, crashed short of runway
SiteLondon Heathrow Airport, United Kingdom
51°27'54(N), −0°,25',54(W)
Aircraft
Aircraft typeBoeing 777-236ER
OperatorBritish Airways
IATA flight No.BA38
ICAO flight No.BAW38
Call signSPEEDBIRD 38
RegistrationG-YMMM
Flight originBeijing Capital International Airport, China
DestinationLondon Heathrow Airport, England, United Kingdom
Occupants152
Passengers136
Crew16
Fatalities0
Injuries47 (1 serious)
Survivors152
A map showing the location of the plane (blue dot) after landing and sliding through the field on the runway safety area – route marked in red

The accident was investigated by the Air Accidents Investigation Branch (AAIB) and a final report was issued in 2010. Ice crystals in the jet fuel were blamed as the cause of the accident, clogging the fuel-oil heat exchanger (FOHE) of each engine. This restricted fuel flow to the engines when thrust was demanded during the final approach to Heathrow.[7] The AAIB then identified the rare problem as specific to Rolls-Royce engine FOHEs and Rolls-Royce developed a modification to its FOHE; the European Aviation Safety Agency (EASA) mandated all affected aircraft to be fitted with the modification before 1 January 2011.[4][8]

Aircraft

 
G-YMMM, the Boeing 777 involved in the accident, photographed in January 2003

The aircraft involved in the accident was a 150-tonne Boeing 777-236ER, registration G-YMMM (manufacturer's serial number 30314, line number 342), powered by two Rolls-Royce Trent 895-17 engines.[9] The aircraft first flew on 18 May 2001 and was delivered to British Airways on 31 May 2001.[10] It had a seating capacity for 233 passengers.[11] On board were 16 crew members and 136 passengers. The crew consisted of Captain Peter Burkill (43), Senior First Officer John Coward (41), First Officer Conor Magenis (35), and 13 cabin crew members. The captain had 12,700 total flight hours, with 8,450 in Boeing 777 aircraft. The senior first officer had 9,000 total flight hours, with 7,000 in Boeing 777 aircraft. The first officer had 5,000 total flight hours, with 1,120 in Boeing 777 aircraft.[12]

Accident

Flight 38 departed from Beijing at 02:09 Greenwich Mean Time (GMT). It flew over Mongolia, Siberia, and Scandinavia, at an altitude between flight level 348 and 400—approximately 34,800 and 40,000 ft (10,600 and 12,200 m), and in temperatures between −74 °C (−101 °F) and −65 °C (−85 °F).[13] Aware of the cold conditions outside, the crew monitored the temperature of the fuel, with the intention of descending to a lower and warmer level if any danger of the fuel freezing arose.[14] This did not prove necessary, as the fuel temperature never dropped below −34 °C (−29 °F), still well above its freezing point.[Note 1]

Although the fuel itself did not freeze, small quantities of water in the fuel did.[Note 2] Ice adhered to the inside of the fuel lines, probably where they ran through the pylons attaching the engines to the wings.[17] This accumulation of ice had no effect on the flight until the final stages of the approach into Heathrow, when increased fuel flow and higher temperatures suddenly released it back into the fuel.[18] This formed a slush of soft ice which flowed forward until it reached the fuel-oil heat exchangers (FOHEs)[Note 3] where it froze once again, causing a restriction in the flow of fuel to the engines.[20][21]

The first symptoms of the fuel-flow restriction were noticed by the flight crew at an altitude of 720 feet (220 m) and 2 miles (3.2 km) from touchdown, when the engines repeatedly failed to respond to a demand for increased thrust from the autothrottle. In attempting to maintain the instrument landing system glide slope, the autopilot sacrificed speed, which reduced to 108 knots (200 km/h; 124 mph) at 200 feet (61 m).[1] The autopilot disconnected at 150 feet (46 m), as the co-pilot took manual control.[4] Meanwhile, the captain reduced the flap setting from 30 to 25° to decrease the drag on the aircraft and stretch the glide.[4][22]

At 12:42, the 777 passed just above traffic on the A30 and the airport's Southern Perimeter road and landed on the grass about 270 metres (890 ft) short of runway 27L.[4] The captain declared an emergency to air traffic control a few seconds before landing. The decision to raise the flaps allowed the plane to miss the ILS beacon within the airport perimeter, thus avoiding more substantial damage.[4]

During the impact and short slide over the ground, the nose gear collapsed, the right main gear separated from the aircraft, penetrating the central fuel tank and cabin space, and the left main gear was pushed up through the wing. The aircraft came to rest on the threshold markings at the start of the runway. A significant amount of fuel leaked, but no fire started.[1] One passenger received serious injuries (concussion and a broken leg), and four crew members and eight passengers received minor injuries.[1][2][3]

Aftermath

The London Ambulance Service stated that three fast response cars, nine ambulances, and several officers were sent to the scene to assess the casualties. Those injured were taken to the nearby Hillingdon Hospital.[23]

Willie Walsh, the British Airways chief executive, released a statement praising the actions of the "flight and cabin crew [who] did a magnificent job and safely evacuated all of the 136 passengers ... The captain of the aircraft is one of our most experienced and has been flying with us for nearly 20 years. Our crews are trained to deal with these situations."[24] He also praised the fire, ambulance, and police services.

All flights in and out of Heathrow were halted for a short time after the accident. When operations resumed, many long-haul outbound flights were either delayed or cancelled, and all short-haul flights were cancelled for the rest of the day. Some inbound flights were delayed, and 24 flights were diverted to Gatwick, Luton, or Stansted. In an attempt to minimise further travel disruptions, Heathrow Airport received dispensation from the Department for Transport to operate some night flights.[2] Even so, the following day (18 January), 113 short-haul flights were cancelled because crews and aircraft were out of position.[25]

On the afternoon of 20 January 2008, two cranes lifted the aircraft onto wheeled platforms and removed it from its resting place.[26] It was towed towards Heathrow's BA maintenance hangars base for storage and further inspections by the AAIB. After assessment of the damage and repair costs, the aircraft was declared to be damaged beyond economic repair (despite still being largely intact) and written off, becoming the first Boeing 777 hull loss in history.[27] It was broken up and scrapped in the spring of 2009. The dismantling and disposal was handled by Air Salvage International.[28]

During a press conference the day after the accident, Captain Peter Burkill said that he would not be publicly commenting on the cause of the incident while the AAIB investigation was in progress. He revealed that Senior First Officer John Coward was flying the aircraft, and that First Officer Conor Magenis was also present on the flight deck at the time of the accident.[29] Coward was more forthcoming in a later interview, stating: "As the final approach started I became aware that there was no power ... suddenly there was nothing from any of the engines, and the plane started to glide."[30]

Burkill and Coward were grounded for a month following the crash while they were assessed for post-traumatic stress disorder. Five months after the accident, Burkill flew again, taking charge of a flight to Montreal, Canada. He remained "haunted" by the incident, and took voluntary redundancy from British Airways in August 2009.[31] Burkill subsequently established a blog and wrote a book, Thirty Seconds to Impact, that denounced BA's treatment of the situation following the crash.[32] In November 2010, Burkill rejoined British Airways, stating, "I am delighted that the discussions with British Airways, have come to a mutually, happy conclusion. In my opinion, British Airways is the pinnacle of any pilot's career, and it is my honour and privilege to be returning to an airline that I joined as a young man."[33]

All 16 crew were awarded the BA Safety Medal for their performance during the accident. The medal is British Airways' highest honour.[34] On 11 December 2008 the crew received the President's Award from the Royal Aeronautical Society.[35]

British Airways continues to use the flight 38 designation on its Beijing to Heathrow route,[36] operating out of Beijing Daxing International Airport, usually with a Boeing 787 Dreamliner.

Initial speculations

Mechanical engine failure was not regarded as a likely cause given the very low probability of a simultaneous dual engine failure.[37] An electronic or software glitch in the computerised engine-control systems was suggested as possible causes of the simultaneous loss of power on both engines.[37] Both engine and computer problems were ruled out by the findings of the February Special Bulletin.[1]

Some speculation indicated that radio interference from the Prime Minister's motorcade, which was leaving Heathrow after dropping the Prime Minister off for a flight to China, was responsible for the accident. This interference was also eliminated as a cause.

Initial analysis from David Learmount, a Flight International editor, was that "The aircraft had either a total or severe power loss and this occurred very late in the final approach because the pilot did not have time to tell air traffic control or passengers." Learmount went on to say that to land in just 350–400 metres (1,150–1,310 ft), the aircraft must have been near stalling when it touched down.[38][39] The captain also reported the aircraft's stall warning system had sounded.[40]

The METAR in force at the time indicated that the wind was forecast to gust according to ICAO criteria for wind reporting,[41] but it was not gusting at the time and wind shear had not been reported.[citation needed] The possibility of a bird strike was raised, but there were no sightings or radar reports of birds.[37] Speculation had focused on electronics and fuel supply issues.[42] A few weeks after the accident, as suspicion started to fall on the possibility of ice in the fuel, United Airlines undertook a review of their procedures for testing and draining the fuel used in their aircraft, while American Airlines considered switching to a different type of jet fuel for polar flights.[43]

Investigation

The Department for Transport's AAIB investigated the accident, with the US National Transportation Safety Board, Boeing, and Rolls-Royce also participating.[4] The investigation took two years to complete, and the AAIB published its final report on 9 February 2010. Three preliminary reports and 18 safety recommendations were issued during the course of the investigation.[4]

The flight data recorder (FDR) and the cockpit voice recorder (CVR), along with the quick access recorder (QAR), were recovered from the aircraft within hours of the accident, and they were transported to the AAIB's Farnborough headquarters, some 30 miles from Heathrow.[44] The information downloaded from these devices confirmed what the crew had already told the investigators, that the engines had not responded when the throttles were advanced during final approach.[45][46]

Fuel system

In its Special Bulletin of 18 February 2008, the AAIB noted evidence that cavitation had taken place in both high-pressure fuel pumps, which could be indicative of a restriction in the fuel supply or excessive aeration of the fuel, although the manufacturer assessed both pumps as still being able to deliver full fuel flow. The report noted the aircraft had flown through air that was unusually cold (but not exceptionally so), and concluded that the temperature had not been low enough to freeze the fuel. Tests were continuing in an attempt to replicate the damage seen in the fuel pumps and to match this to the data recorded on the flight. A comprehensive examination and analysis was to be conducted on the entire aircraft and engine fuel system, including modelling fuel flows, taking account of environmental and aerodynamic effects.

The AAIB issued a further bulletin on 12 May 2008, which confirmed that the investigation continued to focus on fuel delivery. It stated, "The reduction in thrust on both engines was the result of a reduced fuel flow and all engine parameters after the thrust reduction were consistent with this." The report confirmed that the fuel was of good quality and had a freezing point below the coldest temperatures encountered, appearing to rule out fuel freezing as a cause. As in the aforementioned February bulletin, the report noted cavitation damage to the high-pressure fuel pumps of both engines, indicative of abnormally low pressure at the pump inlets. After ruling out fuel freezing or contamination, the investigation then focused on what caused the low pressure at the pump inlets. "Restrictions in the fuel system between the aircraft fuel tanks and each of the engine HP pumps, resulting in reduced fuel flows, is suspected." The fuel delivery system was being investigated at Boeing, and the engines at manufacturer Rolls-Royce in Derby.

The AAIB issued an interim report on 4 September. Offering a tentative conclusion, it stated:[47]

The investigation has shown that fuel to both engines was restricted, most probably due to ice within the fuel feed system. The ice was likely to have formed from water that occurred naturally in the fuel whilst the aircraft operated for a long period, with low fuel flows, in an unusually cold environment, although, G-YMMM was operated within the certified operational envelope at all times.

— AAIB, Interim Report – Boeing 777-236ER, G-YMMM

The report summarised the extensive testing performed in an effort to replicate the problem suffered by G-YMMM. This included creating a mock-up of G-YMMM's fuel delivery system, to which water was added to study its freezing properties. After a battery of tests, the AAIB had not yet succeeded in reproducing the suspected icing behaviour and was undertaking further investigation. Nevertheless, the AAIB believed its testing showed that fuel flow was restricted on G-YMMM and that frozen water in the jet fuel could have caused the restriction, ruling out alternative hypotheses such as a failure of the aircraft's FADEC (computerised engine control system). The hypothesis favoured in the report was that ice had accreted somewhere downstream of the boost pumps in the wing fuel tanks and upstream of the engine-mounted fuel pumps. Either enough ice had accumulated to cause a blockage at a single point, or ice throughout the fuel lines had become dislodged as fuel flow increased during the landing approach, and the dislodged ice had then formed a blockage somewhere downstream.

Because temperatures in flight had not dropped below the 777's designed operating parameters, the AAIB recommended Boeing and Rolls-Royce take interim measures on Trent 800-powered 777s to reduce the risk of ice restricting fuel delivery.[48] Boeing did so by revising the 777 operating procedures so as to reduce the opportunities for such blockages to occur, and by changing the procedure to be followed in the event of power loss to take into account the possibility that ice accumulation was the cause.[7][needs update]

The report went on to recommend that the aviation regulators (FAA and EASA) should consider whether other aircraft types and other engines might be affected by the same problem, and to consider changing the certification process to ensure that future aircraft designs would not be susceptible to the newly recognised danger from ice formation in the fuel.[49]

The report acknowledged that a redesign of the fuel system would not be practical in the near term, and suggested two ways to lower the risk of recurrence. One was to use a fuel additive (FSII) that prevents water ice from forming down to −40 °C (−40 °F). Western air forces have used FSII for decades, and although it is not widely used in commercial aviation, it is nonetheless approved for the 777.

Rejected theories

The Special Bulletin of 18 February, stated "no evidence of a mechanical defect or ingestion of birds or ice" was found, "no evidence of fuel contamination or unusual levels of water content" was seen within the fuel, and the recorded data indicated "no anomalies in the major aircraft systems". Some small foreign bodies, however, were detected in the fuel tanks, although these were later concluded to have had no bearing on the accident.[50]

The Special Bulletin of 12 May 2008 specifically ruled out certain other possible causes, stating: "There is no evidence of a wake vortex encounter, a bird strike, or core engine icing. There is no evidence of any anomalous behaviour of any of the aircraft or engine systems that suggests electromagnetic interference." [51]

Probable cause

The AAIB issued a full report on 9 February 2010. It concluded:

The investigation identified that the reduction in thrust was due to restricted fuel flow to both engines.

The investigation identified the following probable causal factors that led to the fuel flow restrictions:

  1. Accreted ice from within the fuel system released, causing a restriction to the engine fuel flow at the face of the FOHE, on both of the engines.
  2. Ice had formed within the fuel system, from water that occurred naturally in the fuel, whilst the aircraft operated with low fuel flows over a long period and the localised fuel temperatures were in an area described as the 'sticky range'.
  3. The FOHE, although compliant with the applicable certification requirements, was shown to be susceptible to restriction when presented with soft ice in a high concentration, with a fuel temperature that is below −10 °C and a fuel flow above flight idle.
  4. Certification requirements, with which the aircraft and engine fuel systems had to comply, did not take account of this phenomenon as the risk was unrecognised at that time.
    — AAIB, Report on the accident to Boeing 777-236ER, G-YMMM, at London Heathrow Airport on 17 January 2008

Other findings

The AAIB also studied the crashworthiness of the aircraft during the accident sequence. It observed that the main attachment point for the main landing gear was the rear spar of the aircraft's wing; because this spar also formed the rear wall of the main fuel tanks, the crash landing caused the tanks to rupture. Boeing was recommended to redesign the landing gear attachment to reduce the likelihood of fuel loss in similar circumstances.

The report went on to note that the fire extinguisher handles had been manually deployed by the crew before the fuel shut-off switches. The fire extinguisher handles also have the effect of cutting off power to the fuel switches, meaning that the fuel may continue to flow – a potentially dangerous situation. The report restated a previous Boeing Service Bulletin giving procedural advice that fuel switches should be operated before fire handles. It went on: "This was not causal to the accident, but could have had serious consequences in the event of a fire during the evacuation." Indeed, the need to issue Safety Recommendation 2008–2009, affecting all 777 airframes, which had yet to incorporate the Boeing Service Bulletin (SB 777-28-0025) – as was the case with G-YMMM – was given as the main reason for issuing the first special bulletin, well before the accident investigation itself was complete.[1]

Similar incidents

 
Laboratory duplication of ice crystals clogging the FOHE on a Rolls-Royce Trent 800 series engine taken from the NTSB report[7] addressing the incidents of BA Flight 38 and DL Flight 18.
 
N862DA, the aircraft involved in Delta Air Lines Flight 18, seen in 2009

On 26 November 2008, Delta Air Lines Flight 18 from Shanghai to Atlanta, a Trent 895-powered Boeing 777, experienced an "uncommanded rollback" of one engine while in cruise at 39,000 feet (12,000 m). The crew followed manual recovery procedures and the flight continued without incident. The US NTSB assigned one of the investigators who worked on the BA Flight 38 investigation to this incident, and looked specifically for any similarity between the two incidents.[52] The NTSB Safety Recommendation report[53] concluded that ice clogging the FOHE was the likely cause. The evidence was stronger in this case since data from the flight data recorder allowed the investigators to locate where the fuel flow was restricted.

In early 2009, Boeing sent an update to aircraft operators, linking the British Airways and Delta Air Lines "uncommanded rollback" incidents, and identifying the problem as specific to the Rolls-Royce engine FOHEs.[8] Originally, other aircraft were thought to be unaffected by the problem.[8] However, in May 2009, another similar incident happened with an Airbus A330 powered by a Trent series 700 engine.[54]

The enquiries led Boeing to reduce the recommended time that the fuel on 777 aircraft equipped with Rolls-Royce Trent 800-series engines be allowed to remain at temperatures below −10 °C (14 °F) from three to two hours.[55]

On 11 March 2009, the NTSB issued urgent safety recommendation SB-09-11 calling for the redesign of the FOHEs used on Rolls-Royce Trent 800 Series engines. A build-up of ice from water naturally occurring in the fuel had caused a restriction of the flow of fuel to the engines of G-YMMM. Rolls-Royce had already started on redesigning the component, with an in-service date of March 2010 at the latest. All affected engines were to be fitted with the redesigned component within six months of its certification.[56] In May 2010 the Airworthiness Directive was extended to cover the Trent 500 and 700 series engines, as well.[54]

Lawsuit

In November 2009, 10 passengers were announced to be suing Boeing over the incident in the Circuit Court of Cook County in Illinois, United States.[57] Each of the ten plaintiffs reportedly could receive up to US$1,000,000 (about £600,000 at the time) compensation. The lawsuit alleged that the design of the aircraft was "defective and unreasonably dangerous", that Boeing "breached their duty of care", and also breached their "warranties of merchantability and fitness".[58] Claims were settled out of court in 2012.[59]

In popular culture

The Discovery Channel Canada / National Geographic TV series Mayday featured the incident in a season-10 episode titled "The Heathrow Enigma".[60]

See also

Notes

  1. ^ The specification for Jet A-1 fuel requires a maximum freezing point of −47 °C (−53 °F). Depending on its exact composition, the actual freezing point can be lower than this. Subsequent testing found that the fuel on board G-YMMM had a freezing point of −57 °C (−71 °F).[15]
  2. ^ Jet fuel contains water, as a contaminant, in concentrations of up to 100 parts per million.[16]
  3. ^ The FOHE – one per engine – consists of 1,180 small-diameter steel tubes. The fuel flows through the tubes while the hot engine oil circulates around the outside. It is designed to provide two benefits; it warms the fuel to prevent ice reaching other engine components, and simultaneously cools the engine oil.[19]

References

  1. ^ a b c d e f "AAIB Bulletin S1/2008 SPECIAL" (PDF). AAIB. 18 February 2008. (PDF) from the original on 1 June 2012. Retrieved 18 February 2008. ()
  2. ^ a b c "Airliner crash-lands at Heathrow". BBC. 17 January 2008. Retrieved 17 January 2008.
  3. ^ a b Henry, Emma; Britten, Nick (17 January 2008). . The Daily Telegraph. London. Archived from the original on 22 April 2008. Retrieved 26 March 2010.
  4. ^ a b c d e f g h "Report on the accident to Boeing 777-236ER, G-YMMM, at London Heathrow Airport on 17 January 2008". AAIB. Retrieved 9 February 2010.
  5. ^ "Profile: Boeing 777". BBC News. 17 January 2008. Retrieved 17 January 2008.
  6. ^ "Accident to Boeing 777-236, G-YMMM at London Heathrow Airport on 17 January 2008 – Initial Report Update". AAIB. 24 January 2008. Retrieved 24 January 2008.
  7. ^ a b c (PDF). National Transportation Safety Board. 11 March 2009. Archived from the original (PDF) on 23 October 2011.
  8. ^ a b c Croft, John. . Flight Global. Archived from the original on 7 February 2009. Retrieved 3 February 2009.
  9. ^ "Accident description". Aviation-safety.net. 9 February 2010. Retrieved 19 January 2011.
  10. ^ . Archived from the original on 2 August 2010.
  11. ^ AAIB final report, section 1.6.5.1 (page 12) "Cabin Layout"
  12. ^ AAIB final report, section 1.5 (pages 7–8)
  13. ^ AAIB final report, section 1.7.2 (pages 33–34)
  14. ^ AAIB final report, section 1.1 (page 4) "Due to the predicted low temperatures, [the crew] briefed that they would monitor the fuel temperature en route."
  15. ^ AAIB final report, section 1.18.1.1 (pages 117–118)
  16. ^ "A-09-17-18" (PDF). Retrieved 6 July 2013.
  17. ^ AAIB final report, section 2.8.5 (page 155) "Ice accumulation during main tank feed"
  18. ^ AAIB final report, section 2.8.5 (page 155) "Release of accumulated ice on approach"
  19. ^ AAIB final report, section 1.6.8, (page 19)
  20. ^ AAIB final report, section 2.8.5 (page 155) "The fuel flow restriction"
  21. ^ AAIB final report, section 2.8 (page 149)
  22. ^ "BA crash inquiry reveals heroics". BBC. 20 May 2008. Retrieved 20 May 2008.
  23. ^ (Press release). Archived from the original on 25 September 2008.
  24. ^ "Passengers survive as British Airways jet crash lands at Heathrow". The Scotsman. 17 January 2008.
  25. ^ "Latest on Heathrow travel problems". BBC. 18 January 2008. Retrieved 18 January 2008.
  26. ^ "Crashed jet removed from runway". BBC News. 20 January 2008. Retrieved 20 January 2008.
  27. ^ "BA to write off crashed 777". FlightGlobal. 20 February 2008. Retrieved 20 January 2008.
  28. ^ "What happens to a plane wreck?". bbc.co.uk. 13 June 2018. Retrieved 13 June 2018.
  29. ^ "In full: BA crash pilot statement". BBC News. 18 January 2008. Retrieved 19 January 2008.
  30. ^ . Sunday Mirror. 20 January 2008. Archived from the original on 30 January 2009. Retrieved 19 January 2011.
  31. ^ Booth, Jenny (9 February 2010). . The Times. London. Archived from the original on 4 June 2011. Retrieved 27 April 2010.
  32. ^ "Air crash: '30 seconds to impact'". BBC Local (Hereford & Worcester). 24 March 2010. Retrieved 9 November 2011.
  33. ^ Kaminski-Morrow, David. . Flight International. Archived from the original on 1 October 2010. Retrieved 29 September 2010.
  34. ^ . Boarding, Norway. 18 July 2008. Archived from the original on 15 February 2012. Retrieved 10 December 2008.
  35. ^ "RAeS MEDAL WINNERS" (PDF). Royal Aeronautical Society. Retrieved 11 February 2010.
  36. ^ "Flight Aware Live Flight Tracking". Retrieved 17 May 2018.
  37. ^ a b c Woods, Richard; Swinford, Steven; Eddy, Paul (20 January 2008). "Hunt for fatal flaw of Flight 38". The Times. London. Retrieved 26 March 2010.
  38. ^ David Learmount (17 January 2008). . Flightglobal. Archived from the original on 20 May 2011. Retrieved 10 January 2012.
  39. ^ David Learmount (21 January 2008). "British Airways 777 crash landing at Heathrow". Flightglobal. Retrieved 10 January 2012.
  40. ^ "Heathrow Airport Crash investigation – Pilot talks". BBC News. 9 February 2010. Archived from the original on 21 December 2021. Retrieved 8 April 2012 – via YouTube.
  41. ^ EGLL 171220Z 21014KT 180V240 9999 SCT008 BKN010 09/08 Q0997 TEMPO 21018G28KT 4000 RADZ BKN008 – translation here, issued by BAA Heathrow Wunderground.com
  42. ^ . Flight International. 1 February 2008. Archived from the original on 6 April 2013. Retrieved 1 February 2008.
  43. ^ . The Wall Street Journal. 12 February 2008. Archived from the original on 17 February 2008. Retrieved 13 February 2008.
  44. ^ . AAIB. 18 January 2008. Archived from the original on 21 January 2008. Retrieved 11 August 2013. The CVR and FDR have been successfully downloaded at the AAIB laboratories at Farnborough and both records cover the critical final stages of the flight. The QAR was downloaded with the assistance of British Airways and the equipment manufacturer.
  45. ^ . AAIB. 18 January 2008. Archived from the original on 21 January 2008. Retrieved 18 January 2008. Initial indications from the interviews and Flight Recorder analyses show the flight and approach to have progressed normally until the aircraft was established on late finals for Runway 27L. At approximately 600 ft and 2 miles from touch down, the Autothrottle demanded an increase in thrust from the two engines but the engines did not respond. Following further demands for increased thrust from the Autothrottle, and subsequently, the flight crew moving the throttle levers, the engines similarly failed to respond. The aircraft speed reduced and the aircraft descended onto the grass short of the paved runway surface.
  46. ^ "Accident to Boeing 777-236, G-YMMM at London Heathrow Airport on 17 January 2008 – Initial Report Update". AAIB. 24 January 2008. Retrieved 18 January 2008. As previously reported, whilst the aircraft was stabilised on an ILS approach with the autopilot engaged, the autothrust system commanded an increase in thrust from both engines. The engines both initially responded, but after about 3 seconds, the thrust of the right engine reduced. Some eight seconds later the thrust reduced on the left engine to a similar level. The engines did not shut down and both engines continued to produce thrust at an engine speed above flight idle, but less than the commanded thrust.
    Recorded data indicate that an adequate fuel quantity was on board the aircraft and that the autothrottle and engine control commands were performing as expected prior to, and after, the reduction in thrust.
    All possible scenarios that could explain the thrust reduction and continued lack of response of the engines to throttle lever inputs are being examined, in close co-operation with Boeing, Rolls-Royce, and British Airways. This work includes a detailed analysis and examination of the complete fuel flow path from the aircraft tanks to the engine fuel nozzles.
  47. ^ . AAIB. 4 September 2008. Archived from the original on 12 October 2008.
  48. ^ . AAIB. 4 September 2008. Archived from the original on 12 October 2008. Safety Recommendation 2008-047: It is recommended that the Federal Aviation Administration and the European Aviation Safety Agency, in conjunction with Boeing and Rolls-Royce, introduce interim measures for the Boeing 777, powered by Trent 800 engines, to reduce the risk of ice formed from water in aviation turbine fuel causing a restriction in the fuel feed system.
  49. ^ . AAIB. 4 September 2008. Archived from the original on 12 October 2008. Safety Recommendation 2008-048: It is recommended that the Federal Aviation Administration and the European Aviation Safety Agency should take immediate action to consider the implications of the findings of this investigation on other certificated airframe/engine combinations.
    Safety Recommendation 2008-049: It is recommended that the Federal Aviation Administration and the European Aviation Agency review the current certification requirements to ensure that aircraft and engine fuel systems are tolerant to the potential build-up and sudden release of ice in the fuel feed system.
  50. ^ AAIB final report, section 2.3.7 (page 145) "Foreign Object Debris"
  51. ^ AAIB Bulletin S3/2008 Special, AAIB, 12 May 2008, from the original on 18 August 2008
  52. ^ Croft, John (10 December 2008). . Flightglobal. Archived from the original on 25 December 2010. Retrieved 10 December 2008.
  53. ^ Rosenker, Mark V. (11 March 2009). "NTSB Safety Recommendation Number A-09-19-20" (PDF). U.S. NTSB. Retrieved 7 July 2012.
  54. ^ a b (PDF). Federal Aviation Administration. 29 March 2010. p. 1. Archived from the original (PDF) on 19 October 2015.
  55. ^ "Boeing warns of ice problem in some 777 engines". Wings Magazine. Retrieved 17 November 2010.
  56. ^ "NTSB Issues Urgent Safety Recommendation to Address Engine Thrust Rollback Events on B-777 Aircraft" (Press release). NTSB. 11 March 2009. Retrieved 13 March 2009.
  57. ^ "Heathrow crash passengers to sue". BBC News. 19 November 2009. Retrieved 7 January 2010.
  58. ^ Beckford, Martin (19 November 2009). "Heathrow plane crash survivors fight for £1million damages from Boeing in landmark case". The Daily Telegraph. London. Retrieved 20 November 2009.
  59. ^ Millward, David (3 October 2012). "Out of court settlement reached between British Airways passengers and manufacturers". The Daily Telegraph. London. Retrieved 13 July 2013.
  60. ^ "The Heathrow Enigma". Mayday. Season 10. 2011. Discovery Channel Canada / National Geographic Channel.

External links

External video
  "How to Land a Boeing 777 without Any Engines". Smithsonian Channel. 7 October 2013. Archived from the original on 21 December 2021.

  Media related to British Airways Flight BA38 at Wikimedia Commons

  • Air Accidents Investigation Branch Report on the accident to Boeing 777-236ER, G-YMMM, at London Heathrow Airport on 17 January 2008
    • Final Report ()
  • "In Pictures: Heathrow crash-landing". BBC News. BBC. 17 January 2008.
  • "Eyewitnesses on Heathrow incident". BBC News. BBC. 17 January 2008.
  • "Plane passengers 'touched by God'". BBC News. BBC. 18 January 2008.
  • Charig, Francis (8 February 2008). "My escape from BA038 was damn fun". The Daily Telegraph. London.
  • Milmo, Dan (19 January 2008). "Safety fears over crash jet's alarm failure". The Guardian. London. Retrieved 21 January 2008.
  • Accident description at the Aviation Safety Network
  • Audio interviews with Capt Peter Burkill on avweb.com: Part 1 (The Crash) and Part 2 (The Aftermath)
  • August 2010 edition of Flaps Podcast: Interview with Captain Burkill, where he recounted his experience and its aftermath

british, airways, flight, scheduled, international, passenger, flight, from, beijing, capital, international, airport, beijing, china, london, heathrow, airport, london, united, kingdom, kilometre, trip, january, 2008, boeing, 200er, aircraft, operating, fligh. British Airways Flight 38 was a scheduled international passenger flight from Beijing Capital International Airport in Beijing China to London Heathrow Airport in London United Kingdom an 8 100 kilometre 4 400 nmi 5 000 mi trip On 17 January 2008 the Boeing 777 200ER aircraft operating the flight crashed just short of the runway while landing at Heathrow 1 2 3 No fatalities occurred of the 152 people on board 47 sustained injuries one serious 4 It was the first time in the aircraft type s history that a Boeing 777 was declared a hull loss and subsequently written off 5 6 British Airways Flight 38G YMMM after the crash at London Heathrow Airport AccidentDate17 January 2008 2008 01 17 SummaryFuel starvation caused by ice in the fuel oil heat exchangers crashed short of runwaySiteLondon Heathrow Airport United Kingdom 51 27 54 N 0 25 54 W AircraftAircraft typeBoeing 777 236EROperatorBritish AirwaysIATA flight No BA38ICAO flight No BAW38Call signSPEEDBIRD 38RegistrationG YMMMFlight originBeijing Capital International Airport ChinaDestinationLondon Heathrow Airport England United KingdomOccupants152Passengers136Crew16Fatalities0Injuries47 1 serious Survivors152A map showing the location of the plane blue dot after landing and sliding through the field on the runway safety area route marked in red The accident was investigated by the Air Accidents Investigation Branch AAIB and a final report was issued in 2010 Ice crystals in the jet fuel were blamed as the cause of the accident clogging the fuel oil heat exchanger FOHE of each engine This restricted fuel flow to the engines when thrust was demanded during the final approach to Heathrow 7 The AAIB then identified the rare problem as specific to Rolls Royce engine FOHEs and Rolls Royce developed a modification to its FOHE the European Aviation Safety Agency EASA mandated all affected aircraft to be fitted with the modification before 1 January 2011 4 8 Contents 1 Aircraft 2 Accident 3 Aftermath 4 Initial speculations 5 Investigation 5 1 Fuel system 5 2 Rejected theories 5 3 Probable cause 5 4 Other findings 6 Similar incidents 7 Lawsuit 8 In popular culture 9 See also 10 Notes 11 References 12 External linksAircraft Edit G YMMM the Boeing 777 involved in the accident photographed in January 2003 The aircraft involved in the accident was a 150 tonne Boeing 777 236ER registration G YMMM manufacturer s serial number 30314 line number 342 powered by two Rolls Royce Trent 895 17 engines 9 The aircraft first flew on 18 May 2001 and was delivered to British Airways on 31 May 2001 10 It had a seating capacity for 233 passengers 11 On board were 16 crew members and 136 passengers The crew consisted of Captain Peter Burkill 43 Senior First Officer John Coward 41 First Officer Conor Magenis 35 and 13 cabin crew members The captain had 12 700 total flight hours with 8 450 in Boeing 777 aircraft The senior first officer had 9 000 total flight hours with 7 000 in Boeing 777 aircraft The first officer had 5 000 total flight hours with 1 120 in Boeing 777 aircraft 12 Accident EditFlight 38 departed from Beijing at 02 09 Greenwich Mean Time GMT It flew over Mongolia Siberia and Scandinavia at an altitude between flight level 348 and 400 approximately 34 800 and 40 000 ft 10 600 and 12 200 m and in temperatures between 74 C 101 F and 65 C 85 F 13 Aware of the cold conditions outside the crew monitored the temperature of the fuel with the intention of descending to a lower and warmer level if any danger of the fuel freezing arose 14 This did not prove necessary as the fuel temperature never dropped below 34 C 29 F still well above its freezing point Note 1 Although the fuel itself did not freeze small quantities of water in the fuel did Note 2 Ice adhered to the inside of the fuel lines probably where they ran through the pylons attaching the engines to the wings 17 This accumulation of ice had no effect on the flight until the final stages of the approach into Heathrow when increased fuel flow and higher temperatures suddenly released it back into the fuel 18 This formed a slush of soft ice which flowed forward until it reached the fuel oil heat exchangers FOHEs Note 3 where it froze once again causing a restriction in the flow of fuel to the engines 20 21 The first symptoms of the fuel flow restriction were noticed by the flight crew at an altitude of 720 feet 220 m and 2 miles 3 2 km from touchdown when the engines repeatedly failed to respond to a demand for increased thrust from the autothrottle In attempting to maintain the instrument landing system glide slope the autopilot sacrificed speed which reduced to 108 knots 200 km h 124 mph at 200 feet 61 m 1 The autopilot disconnected at 150 feet 46 m as the co pilot took manual control 4 Meanwhile the captain reduced the flap setting from 30 to 25 to decrease the drag on the aircraft and stretch the glide 4 22 At 12 42 the 777 passed just above traffic on the A30 and the airport s Southern Perimeter road and landed on the grass about 270 metres 890 ft short of runway 27L 4 The captain declared an emergency to air traffic control a few seconds before landing The decision to raise the flaps allowed the plane to miss the ILS beacon within the airport perimeter thus avoiding more substantial damage 4 During the impact and short slide over the ground the nose gear collapsed the right main gear separated from the aircraft penetrating the central fuel tank and cabin space and the left main gear was pushed up through the wing The aircraft came to rest on the threshold markings at the start of the runway A significant amount of fuel leaked but no fire started 1 One passenger received serious injuries concussion and a broken leg and four crew members and eight passengers received minor injuries 1 2 3 Aftermath EditThe London Ambulance Service stated that three fast response cars nine ambulances and several officers were sent to the scene to assess the casualties Those injured were taken to the nearby Hillingdon Hospital 23 Willie Walsh the British Airways chief executive released a statement praising the actions of the flight and cabin crew who did a magnificent job and safely evacuated all of the 136 passengers The captain of the aircraft is one of our most experienced and has been flying with us for nearly 20 years Our crews are trained to deal with these situations 24 He also praised the fire ambulance and police services All flights in and out of Heathrow were halted for a short time after the accident When operations resumed many long haul outbound flights were either delayed or cancelled and all short haul flights were cancelled for the rest of the day Some inbound flights were delayed and 24 flights were diverted to Gatwick Luton or Stansted In an attempt to minimise further travel disruptions Heathrow Airport received dispensation from the Department for Transport to operate some night flights 2 Even so the following day 18 January 113 short haul flights were cancelled because crews and aircraft were out of position 25 On the afternoon of 20 January 2008 two cranes lifted the aircraft onto wheeled platforms and removed it from its resting place 26 It was towed towards Heathrow s BA maintenance hangars base for storage and further inspections by the AAIB After assessment of the damage and repair costs the aircraft was declared to be damaged beyond economic repair despite still being largely intact and written off becoming the first Boeing 777 hull loss in history 27 It was broken up and scrapped in the spring of 2009 The dismantling and disposal was handled by Air Salvage International 28 During a press conference the day after the accident Captain Peter Burkill said that he would not be publicly commenting on the cause of the incident while the AAIB investigation was in progress He revealed that Senior First Officer John Coward was flying the aircraft and that First Officer Conor Magenis was also present on the flight deck at the time of the accident 29 Coward was more forthcoming in a later interview stating As the final approach started I became aware that there was no power suddenly there was nothing from any of the engines and the plane started to glide 30 Burkill and Coward were grounded for a month following the crash while they were assessed for post traumatic stress disorder Five months after the accident Burkill flew again taking charge of a flight to Montreal Canada He remained haunted by the incident and took voluntary redundancy from British Airways in August 2009 31 Burkill subsequently established a blog and wrote a book Thirty Seconds to Impact that denounced BA s treatment of the situation following the crash 32 In November 2010 Burkill rejoined British Airways stating I am delighted that the discussions with British Airways have come to a mutually happy conclusion In my opinion British Airways is the pinnacle of any pilot s career and it is my honour and privilege to be returning to an airline that I joined as a young man 33 All 16 crew were awarded the BA Safety Medal for their performance during the accident The medal is British Airways highest honour 34 On 11 December 2008 the crew received the President s Award from the Royal Aeronautical Society 35 British Airways continues to use the flight 38 designation on its Beijing to Heathrow route 36 operating out of Beijing Daxing International Airport usually with a Boeing 787 Dreamliner Initial speculations EditMechanical engine failure was not regarded as a likely cause given the very low probability of a simultaneous dual engine failure 37 An electronic or software glitch in the computerised engine control systems was suggested as possible causes of the simultaneous loss of power on both engines 37 Both engine and computer problems were ruled out by the findings of the February Special Bulletin 1 Some speculation indicated that radio interference from the Prime Minister s motorcade which was leaving Heathrow after dropping the Prime Minister off for a flight to China was responsible for the accident This interference was also eliminated as a cause Initial analysis from David Learmount a Flight International editor was that The aircraft had either a total or severe power loss and this occurred very late in the final approach because the pilot did not have time to tell air traffic control or passengers Learmount went on to say that to land in just 350 400 metres 1 150 1 310 ft the aircraft must have been near stalling when it touched down 38 39 The captain also reported the aircraft s stall warning system had sounded 40 The METAR in force at the time indicated that the wind was forecast to gust according to ICAO criteria for wind reporting 41 but it was not gusting at the time and wind shear had not been reported citation needed The possibility of a bird strike was raised but there were no sightings or radar reports of birds 37 Speculation had focused on electronics and fuel supply issues 42 A few weeks after the accident as suspicion started to fall on the possibility of ice in the fuel United Airlines undertook a review of their procedures for testing and draining the fuel used in their aircraft while American Airlines considered switching to a different type of jet fuel for polar flights 43 Investigation EditThe Department for Transport s AAIB investigated the accident with the US National Transportation Safety Board Boeing and Rolls Royce also participating 4 The investigation took two years to complete and the AAIB published its final report on 9 February 2010 Three preliminary reports and 18 safety recommendations were issued during the course of the investigation 4 The flight data recorder FDR and the cockpit voice recorder CVR along with the quick access recorder QAR were recovered from the aircraft within hours of the accident and they were transported to the AAIB s Farnborough headquarters some 30 miles from Heathrow 44 The information downloaded from these devices confirmed what the crew had already told the investigators that the engines had not responded when the throttles were advanced during final approach 45 46 Fuel system Edit In its Special Bulletin of 18 February 2008 the AAIB noted evidence that cavitation had taken place in both high pressure fuel pumps which could be indicative of a restriction in the fuel supply or excessive aeration of the fuel although the manufacturer assessed both pumps as still being able to deliver full fuel flow The report noted the aircraft had flown through air that was unusually cold but not exceptionally so and concluded that the temperature had not been low enough to freeze the fuel Tests were continuing in an attempt to replicate the damage seen in the fuel pumps and to match this to the data recorded on the flight A comprehensive examination and analysis was to be conducted on the entire aircraft and engine fuel system including modelling fuel flows taking account of environmental and aerodynamic effects The AAIB issued a further bulletin on 12 May 2008 which confirmed that the investigation continued to focus on fuel delivery It stated The reduction in thrust on both engines was the result of a reduced fuel flow and all engine parameters after the thrust reduction were consistent with this The report confirmed that the fuel was of good quality and had a freezing point below the coldest temperatures encountered appearing to rule out fuel freezing as a cause As in the aforementioned February bulletin the report noted cavitation damage to the high pressure fuel pumps of both engines indicative of abnormally low pressure at the pump inlets After ruling out fuel freezing or contamination the investigation then focused on what caused the low pressure at the pump inlets Restrictions in the fuel system between the aircraft fuel tanks and each of the engine HP pumps resulting in reduced fuel flows is suspected The fuel delivery system was being investigated at Boeing and the engines at manufacturer Rolls Royce in Derby The AAIB issued an interim report on 4 September Offering a tentative conclusion it stated 47 The investigation has shown that fuel to both engines was restricted most probably due to ice within the fuel feed system The ice was likely to have formed from water that occurred naturally in the fuel whilst the aircraft operated for a long period with low fuel flows in an unusually cold environment although G YMMM was operated within the certified operational envelope at all times AAIB Interim Report Boeing 777 236ER G YMMM The report summarised the extensive testing performed in an effort to replicate the problem suffered by G YMMM This included creating a mock up of G YMMM s fuel delivery system to which water was added to study its freezing properties After a battery of tests the AAIB had not yet succeeded in reproducing the suspected icing behaviour and was undertaking further investigation Nevertheless the AAIB believed its testing showed that fuel flow was restricted on G YMMM and that frozen water in the jet fuel could have caused the restriction ruling out alternative hypotheses such as a failure of the aircraft s FADEC computerised engine control system The hypothesis favoured in the report was that ice had accreted somewhere downstream of the boost pumps in the wing fuel tanks and upstream of the engine mounted fuel pumps Either enough ice had accumulated to cause a blockage at a single point or ice throughout the fuel lines had become dislodged as fuel flow increased during the landing approach and the dislodged ice had then formed a blockage somewhere downstream Because temperatures in flight had not dropped below the 777 s designed operating parameters the AAIB recommended Boeing and Rolls Royce take interim measures on Trent 800 powered 777s to reduce the risk of ice restricting fuel delivery 48 Boeing did so by revising the 777 operating procedures so as to reduce the opportunities for such blockages to occur and by changing the procedure to be followed in the event of power loss to take into account the possibility that ice accumulation was the cause 7 needs update The report went on to recommend that the aviation regulators FAA and EASA should consider whether other aircraft types and other engines might be affected by the same problem and to consider changing the certification process to ensure that future aircraft designs would not be susceptible to the newly recognised danger from ice formation in the fuel 49 The report acknowledged that a redesign of the fuel system would not be practical in the near term and suggested two ways to lower the risk of recurrence One was to use a fuel additive FSII that prevents water ice from forming down to 40 C 40 F Western air forces have used FSII for decades and although it is not widely used in commercial aviation it is nonetheless approved for the 777 Rejected theories Edit The Special Bulletin of 18 February stated no evidence of a mechanical defect or ingestion of birds or ice was found no evidence of fuel contamination or unusual levels of water content was seen within the fuel and the recorded data indicated no anomalies in the major aircraft systems Some small foreign bodies however were detected in the fuel tanks although these were later concluded to have had no bearing on the accident 50 The Special Bulletin of 12 May 2008 specifically ruled out certain other possible causes stating There is no evidence of a wake vortex encounter a bird strike or core engine icing There is no evidence of any anomalous behaviour of any of the aircraft or engine systems that suggests electromagnetic interference 51 Probable cause Edit The AAIB issued a full report on 9 February 2010 It concluded The investigation identified that the reduction in thrust was due to restricted fuel flow to both engines The investigation identified the following probable causal factors that led to the fuel flow restrictions Accreted ice from within the fuel system released causing a restriction to the engine fuel flow at the face of the FOHE on both of the engines Ice had formed within the fuel system from water that occurred naturally in the fuel whilst the aircraft operated with low fuel flows over a long period and the localised fuel temperatures were in an area described as the sticky range The FOHE although compliant with the applicable certification requirements was shown to be susceptible to restriction when presented with soft ice in a high concentration with a fuel temperature that is below 10 C and a fuel flow above flight idle Certification requirements with which the aircraft and engine fuel systems had to comply did not take account of this phenomenon as the risk was unrecognised at that time AAIB Report on the accident to Boeing 777 236ER G YMMM at London Heathrow Airport on 17 January 2008 Other findings Edit The AAIB also studied the crashworthiness of the aircraft during the accident sequence It observed that the main attachment point for the main landing gear was the rear spar of the aircraft s wing because this spar also formed the rear wall of the main fuel tanks the crash landing caused the tanks to rupture Boeing was recommended to redesign the landing gear attachment to reduce the likelihood of fuel loss in similar circumstances The report went on to note that the fire extinguisher handles had been manually deployed by the crew before the fuel shut off switches The fire extinguisher handles also have the effect of cutting off power to the fuel switches meaning that the fuel may continue to flow a potentially dangerous situation The report restated a previous Boeing Service Bulletin giving procedural advice that fuel switches should be operated before fire handles It went on This was not causal to the accident but could have had serious consequences in the event of a fire during the evacuation Indeed the need to issue Safety Recommendation 2008 2009 affecting all 777 airframes which had yet to incorporate the Boeing Service Bulletin SB 777 28 0025 as was the case with G YMMM was given as the main reason for issuing the first special bulletin well before the accident investigation itself was complete 1 Similar incidents Edit Laboratory duplication of ice crystals clogging the FOHE on a Rolls Royce Trent 800 series engine taken from the NTSB report 7 addressing the incidents of BA Flight 38 and DL Flight 18 N862DA the aircraft involved in Delta Air Lines Flight 18 seen in 2009 On 26 November 2008 Delta Air Lines Flight 18 from Shanghai to Atlanta a Trent 895 powered Boeing 777 experienced an uncommanded rollback of one engine while in cruise at 39 000 feet 12 000 m The crew followed manual recovery procedures and the flight continued without incident The US NTSB assigned one of the investigators who worked on the BA Flight 38 investigation to this incident and looked specifically for any similarity between the two incidents 52 The NTSB Safety Recommendation report 53 concluded that ice clogging the FOHE was the likely cause The evidence was stronger in this case since data from the flight data recorder allowed the investigators to locate where the fuel flow was restricted In early 2009 Boeing sent an update to aircraft operators linking the British Airways and Delta Air Lines uncommanded rollback incidents and identifying the problem as specific to the Rolls Royce engine FOHEs 8 Originally other aircraft were thought to be unaffected by the problem 8 However in May 2009 another similar incident happened with an Airbus A330 powered by a Trent series 700 engine 54 The enquiries led Boeing to reduce the recommended time that the fuel on 777 aircraft equipped with Rolls Royce Trent 800 series engines be allowed to remain at temperatures below 10 C 14 F from three to two hours 55 On 11 March 2009 the NTSB issued urgent safety recommendation SB 09 11 calling for the redesign of the FOHEs used on Rolls Royce Trent 800 Series engines A build up of ice from water naturally occurring in the fuel had caused a restriction of the flow of fuel to the engines of G YMMM Rolls Royce had already started on redesigning the component with an in service date of March 2010 at the latest All affected engines were to be fitted with the redesigned component within six months of its certification 56 In May 2010 the Airworthiness Directive was extended to cover the Trent 500 and 700 series engines as well 54 Lawsuit EditIn November 2009 10 passengers were announced to be suing Boeing over the incident in the Circuit Court of Cook County in Illinois United States 57 Each of the ten plaintiffs reportedly could receive up to US 1 000 000 about 600 000 at the time compensation The lawsuit alleged that the design of the aircraft was defective and unreasonably dangerous that Boeing breached their duty of care and also breached their warranties of merchantability and fitness 58 Claims were settled out of court in 2012 59 In popular culture EditThe Discovery Channel Canada National Geographic TV series Mayday featured the incident in a season 10 episode titled The Heathrow Enigma 60 See also Edit London portal Aviation portalAviation safety Cathay Pacific Flight 780 an Airbus A330 that lost engine control shortly before landing at Hong Kong International Airport in 2010 British Airways Flight 9 a Boeing 747 that lost all engine control List of accidents and incidents involving commercial aircraft Runway safety area Scandinavian Airlines Flight 751Notes Edit The specification for Jet A 1 fuel requires a maximum freezing point of 47 C 53 F Depending on its exact composition the actual freezing point can be lower than this Subsequent testing found that the fuel on board G YMMM had a freezing point of 57 C 71 F 15 Jet fuel contains water as a contaminant in concentrations of up to 100 parts per million 16 The FOHE one per engine consists of 1 180 small diameter steel tubes The fuel flows through the tubes while the hot engine oil circulates around the outside It is designed to provide two benefits it warms the fuel to prevent ice reaching other engine components and simultaneously cools the engine oil 19 References Edit a b c d e f AAIB Bulletin S1 2008 SPECIAL PDF AAIB 18 February 2008 Archived PDF from the original on 1 June 2012 Retrieved 18 February 2008 a b c Airliner crash lands at Heathrow BBC 17 January 2008 Retrieved 17 January 2008 a b Henry Emma Britten Nick 17 January 2008 Heathrow plane crash pilot lost all power The Daily Telegraph London Archived from the original on 22 April 2008 Retrieved 26 March 2010 a b c d e f g h Report on the accident to Boeing 777 236ER G YMMM at London Heathrow Airport on 17 January 2008 AAIB Retrieved 9 February 2010 Profile Boeing 777 BBC News 17 January 2008 Retrieved 17 January 2008 Accident to Boeing 777 236 G YMMM at London Heathrow Airport on 17 January 2008 Initial Report Update AAIB 24 January 2008 Retrieved 24 January 2008 a b c Safety Recommendation A 09 17 and 18 PDF National Transportation Safety Board 11 March 2009 Archived from the original PDF on 23 October 2011 a b c Croft John Boeing links Heathrow Atlanta Trent 895 engine rollbacks Flight Global Archived from the original on 7 February 2009 Retrieved 3 February 2009 Accident description Aviation safety net 9 February 2010 Retrieved 19 January 2011 G YMMM British Airways Boeing 777 236 ER cn 30314 ln 342 Planespotters net Just Aviation Archived from the original on 2 August 2010 AAIB final report section 1 6 5 1 page 12 Cabin Layout AAIB final report section 1 5 pages 7 8 AAIB final report section 1 7 2 pages 33 34 AAIB final report section 1 1 page 4 Due to the predicted low temperatures the crew briefed that they would monitor the fuel temperature en route AAIB final report section 1 18 1 1 pages 117 118 A 09 17 18 PDF Retrieved 6 July 2013 AAIB final report section 2 8 5 page 155 Ice accumulation during main tank feed AAIB final report section 2 8 5 page 155 Release of accumulated ice on approach AAIB final report section 1 6 8 page 19 AAIB final report section 2 8 5 page 155 The fuel flow restriction AAIB final report section 2 8 page 149 BA crash inquiry reveals heroics BBC 20 May 2008 Retrieved 20 May 2008 News Release Call to Heathrow Airport Press release Archived from the original on 25 September 2008 Passengers survive as British Airways jet crash lands at Heathrow The Scotsman 17 January 2008 Latest on Heathrow travel problems BBC 18 January 2008 Retrieved 18 January 2008 Crashed jet removed from runway BBC News 20 January 2008 Retrieved 20 January 2008 BA to write off crashed 777 FlightGlobal 20 February 2008 Retrieved 20 January 2008 What happens to a plane wreck bbc co uk 13 June 2018 Retrieved 13 June 2018 In full BA crash pilot statement BBC News 18 January 2008 Retrieved 19 January 2008 Heathrow crash co pilot John Coward I thought we d die Sunday Mirror 20 January 2008 Archived from the original on 30 January 2009 Retrieved 19 January 2011 Booth Jenny 9 February 2010 Pilot of BA jet said goodbye to wife in final moments of Heathrow crash The Times London Archived from the original on 4 June 2011 Retrieved 27 April 2010 Air crash 30 seconds to impact BBC Local Hereford amp Worcester 24 March 2010 Retrieved 9 November 2011 Kaminski Morrow David British Airways to rehire captain of crashed 777 Flight International Archived from the original on 1 October 2010 Retrieved 29 September 2010 Exceptional honour for BA38 crew Boarding Norway 18 July 2008 Archived from the original on 15 February 2012 Retrieved 10 December 2008 RAeS MEDAL WINNERS PDF Royal Aeronautical Society Retrieved 11 February 2010 Flight Aware Live Flight Tracking Retrieved 17 May 2018 a b c Woods Richard Swinford Steven Eddy Paul 20 January 2008 Hunt for fatal flaw of Flight 38 The Times London Retrieved 26 March 2010 David Learmount 17 January 2008 VIDEO amp GRAPHIC Flight s safety editor David Learmount gives his account of what happened to the BA Boeing 777 that crash landed at Heathrow Flightglobal Archived from the original on 20 May 2011 Retrieved 10 January 2012 David Learmount 21 January 2008 British Airways 777 crash landing at Heathrow Flightglobal Retrieved 10 January 2012 Heathrow Airport Crash investigation Pilot talks BBC News 9 February 2010 Archived from the original on 21 December 2021 Retrieved 8 April 2012 via YouTube EGLL 171220Z 21014KT 180V240 9999 SCT008 BKN010 09 08 Q0997 TEMPO 21018G28KT 4000 RADZ BKN008 translation here issued by BAA Heathrow Wunderground com Leaked Detailed BA 777 Accident Investigation Update Flight International 1 February 2008 Archived from the original on 6 April 2013 Retrieved 1 February 2008 United American Plan Safety Push After Icing Linked to British Crash The Wall Street Journal 12 February 2008 Archived from the original on 17 February 2008 Retrieved 13 February 2008 Accident to Boeing 777 236 G YMMM at London Heathrow Airport on 17 January 2008 Initial Report AAIB 18 January 2008 Archived from the original on 21 January 2008 Retrieved 11 August 2013 The CVR and FDR have been successfully downloaded at the AAIB laboratories at Farnborough and both records cover the critical final stages of the flight The QAR was downloaded with the assistance of British Airways and the equipment manufacturer Accident to Boeing 777 236 G YMMM at London Heathrow Airport on 17 January 2008 Initial Report AAIB 18 January 2008 Archived from the original on 21 January 2008 Retrieved 18 January 2008 Initial indications from the interviews and Flight Recorder analyses show the flight and approach to have progressed normally until the aircraft was established on late finals for Runway 27L At approximately 600 ft and 2 miles from touch down the Autothrottle demanded an increase in thrust from the two engines but the engines did not respond Following further demands for increased thrust from the Autothrottle and subsequently the flight crew moving the throttle levers the engines similarly failed to respond The aircraft speed reduced and the aircraft descended onto the grass short of the paved runway surface Accident to Boeing 777 236 G YMMM at London Heathrow Airport on 17 January 2008 Initial Report Update AAIB 24 January 2008 Retrieved 18 January 2008 As previously reported whilst the aircraft was stabilised on an ILS approach with the autopilot engaged the autothrust system commanded an increase in thrust from both engines The engines both initially responded but after about 3 seconds the thrust of the right engine reduced Some eight seconds later the thrust reduced on the left engine to a similar level The engines did not shut down and both engines continued to produce thrust at an engine speed above flight idle but less than the commanded thrust Recorded data indicate that an adequate fuel quantity was on board the aircraft and that the autothrottle and engine control commands were performing as expected prior to and after the reduction in thrust All possible scenarios that could explain the thrust reduction and continued lack of response of the engines to throttle lever inputs are being examined in close co operation with Boeing Rolls Royce and British Airways This work includes a detailed analysis and examination of the complete fuel flow path from the aircraft tanks to the engine fuel nozzles Interim Report Boeing 777 236ER G YMMM AAIB 4 September 2008 Archived from the original on 12 October 2008 Interim Report Boeing 777 236ER G YMMM AAIB 4 September 2008 Archived from the original on 12 October 2008 Safety Recommendation 2008 047 It is recommended that the Federal Aviation Administration and the European Aviation Safety Agency in conjunction with Boeing and Rolls Royce introduce interim measures for the Boeing 777 powered by Trent 800 engines to reduce the risk of ice formed from water in aviation turbine fuel causing a restriction in the fuel feed system Interim Report Boeing 777 236ER G YMMM AAIB 4 September 2008 Archived from the original on 12 October 2008 Safety Recommendation 2008 048 It is recommended that the Federal Aviation Administration and the European Aviation Safety Agency should take immediate action to consider the implications of the findings of this investigation on other certificated airframe engine combinations Safety Recommendation 2008 049 It is recommended that the Federal Aviation Administration and the European Aviation Agency review the current certification requirements to ensure that aircraft and engine fuel systems are tolerant to the potential build up and sudden release of ice in the fuel feed system AAIB final report section 2 3 7 page 145 Foreign Object Debris AAIB Bulletin S3 2008 Special AAIB 12 May 2008 archived from the original on 18 August 2008 Croft John 10 December 2008 NTSB investigates Heathrow like Trent 800 engine issue Flightglobal Archived from the original on 25 December 2010 Retrieved 10 December 2008 Rosenker Mark V 11 March 2009 NTSB Safety Recommendation Number A 09 19 20 PDF U S NTSB Retrieved 7 July 2012 a b Airworthiness Directives Rolls Royce plc RB211 Trent 500 700 and 800 Series Turbofan Engines PDF Federal Aviation Administration 29 March 2010 p 1 Archived from the original PDF on 19 October 2015 Boeing warns of ice problem in some 777 engines Wings Magazine Retrieved 17 November 2010 NTSB Issues Urgent Safety Recommendation to Address Engine Thrust Rollback Events on B 777 Aircraft Press release NTSB 11 March 2009 Retrieved 13 March 2009 Heathrow crash passengers to sue BBC News 19 November 2009 Retrieved 7 January 2010 Beckford Martin 19 November 2009 Heathrow plane crash survivors fight for 1million damages from Boeing in landmark case The Daily Telegraph London Retrieved 20 November 2009 Millward David 3 October 2012 Out of court settlement reached between British Airways passengers and manufacturers The Daily Telegraph London Retrieved 13 July 2013 The Heathrow Enigma Mayday Season 10 2011 Discovery Channel Canada National Geographic Channel External links EditExternal video How to Land a Boeing 777 without Any Engines Smithsonian Channel 7 October 2013 Archived from the original on 21 December 2021 Media related to British Airways Flight BA38 at Wikimedia Commons Air Accidents Investigation Branch Report on the accident to Boeing 777 236ER G YMMM at London Heathrow Airport on 17 January 2008 Final Report Archive In Pictures Heathrow crash landing BBC News BBC 17 January 2008 Eyewitnesses on Heathrow incident BBC News BBC 17 January 2008 Plane passengers touched by God BBC News BBC 18 January 2008 Charig Francis 8 February 2008 My escape from BA038 was damn fun The Daily Telegraph London Milmo Dan 19 January 2008 Safety fears over crash jet s alarm failure The Guardian London Retrieved 21 January 2008 Accident description at the Aviation Safety Network Audio interviews with Capt Peter Burkill on avweb com Part 1 The Crash and Part 2 The Aftermath August 2010 edition of Flaps Podcast Interview with Captain Burkill where he recounted his experience and its aftermath Retrieved from https en wikipedia org w index php title British Airways Flight 38 amp oldid 1129032702, wikipedia, wiki, book, books, library,

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