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Boeing 737 rudder issues

During the 1990s, a series of issues affecting the rudder of Boeing 737 passenger aircraft resulted in multiple incidents. In two separate accidents, pilots lost control of their aircraft due to a sudden and unexpected rudder movement, and the resulting crashes killed everyone on board, 157 people in total.[1] Similar rudder issues led to a temporary loss of control on at least one other Boeing 737 flight before the cause of the problem was ultimately identified.

The National Transportation Safety Board determined that the incidents were the result of a design flaw that could result in an uncommanded movement of the aircraft's rudder.[2]: 13 [3]: ix 

The issues were resolved after the Federal Aviation Administration ordered modifications for all Boeing 737 aircraft in service. In 2016, former NTSB investigator John Cox stated that time has proven the NTSB correct in its findings because no additional rudder-reversal incidents have occurred since Boeing's redesign.[4]

Rudder function

Unlike other twin-engine large transport aircraft in service at the time, the Boeing 737 was designed with a single rudder panel and single rudder actuator.[2]: 14  The single rudder panel is controlled by a single hydraulic Power Control Unit (PCU).[2]: 13  Inside the PCU is a dual servo valve that, based on input from the pilot's rudder pedals or the aircraft's yaw damper system, directs the flow of hydraulic fluid in order to move the rudder.[2]: 19  The PCU for affected Boeing 737 aircraft was designed by Boeing and manufactured by Parker Hannifin.[2]: 20 

First accident and investigation

On March 3, 1991, United Airlines Flight 585, a Boeing 737-200, crashed while attempting to land in Colorado Springs, Colorado. During the airplane's landing approach, the plane rolled to the right and pitched nose-down into a near-vertical dive.[2]: ix  The resulting crash destroyed the aircraft and killed all 25 people on board.[2]: ix 

Although the NTSB investigated the accident, it was unable to conclusively identify the cause of the crash. The rudder PCU from Flight 585 was severely damaged, which prevented operational testing of the PCU.[3]: 47  A review of the flight crew's history determined that Flight 585's captain strictly adhered to operating procedures and had a conservative approach to flying.[3]: 47  A first officer who had previously flown with Flight 585's captain reported that the captain had indicated to him while landing in turbulent weather that the captain had no problem with declaring a go-around if the landing appeared unsafe.[3]: 48  The first officer was considered to be "very competent" by the captain on previous trips they had flown together.[3]: 48  The weather data available to the NTSB indicated that Flight 585 might have encountered a horizontal-axis wind vortex that could have caused the aircraft to roll over, but this could not be shown conclusively to have happened or to have caused the rollover.[3]: 48–49 

On December 8, 1992, the NTSB published a report that identified what the NTSB believed at the time to be the two most likely causes of the accident. The first possibility was that the airplane's directional control system had malfunctioned and caused the rudder to move in a manner that caused the accident. The second possibility was a weather disturbance that caused a sudden rudder movement or loss of control. The Board determined that it lacked sufficient evidence to conclude either theory as the probable cause of the accident.[2]: ix [3]: 49  This was only the fourth time in the NTSB's history that it had closed an investigation and published a final aircraft accident report where the probable cause was undetermined.[5]

Second accident

On September 8, 1994, USAir Flight 427, a Boeing 737-300, crashed near Pittsburgh, Pennsylvania. While on approach to Pittsburgh International Airport, Flight 427 suddenly rolled to the left. Although the pilots were briefly able to roll right and level the plane, it rolled left a second time and the pilots were unable to recover.[3]: 4  The resulting crash killed all 132 people on board.[3]: 9  The NTSB realized early into its investigation that the crash of Flight 427 might have been caused by an unintended or uncommanded rudder movement, similar to the suspected (but not yet established) cause of the Flight 585 crash.[3]: 44  As a result, the NTSB conducted additional testing on United Flight 585's Parker-Hannifin PCU servo during its Flight 427 investigation.[2]: 73 

One of the problems facing investigators was the relative lack of precision in the data produced by the flight data recorder (FDR), which only recorded control inputs at periodic intervals with significant time gaps between samples, gaps during which no data was recorded no matter what the pilot did with the controls. This lack of precision led to it being possible for Boeing to interpret the data differently from the way the NTSB did, leading the manufacturer to suspect and insist that the pilot had responded incorrectly to a wake turbulence incident.[6]

At the request of the NTSB, data from the Penny & Giles quick access recorder (QAR) of a British Airways (BA) Boeing 747-400 was supplied to the NTSB by BA. The data was from a London-Bangkok flight in which the aircraft suffered an uncommanded elevator movement and momentary elevator reversal on take-off, the aircraft then landed safely. Operating alongside the FDR system, the QAR on BA's 747-400s, in conjunction with a Data Management Unit, received and recorded more aircraft parametric data, including control input values at a higher rate.[7] This BA data led to renewed suspicion of the similar valve design used on the 737 rudder. As a result of this earlier BA incident, Boeing had, in fact, modified the design of the 747 elevator servo system, and the modified system had been retroactively fitted to all 747-400s in service.[6]

Eastwind incident

On June 9, 1996, while the NTSB's investigation of Flight 427 was still ongoing, the pilots of Eastwind Airlines Flight 517 briefly lost control of their aircraft, a 737-200, while flying from Trenton, New Jersey, to Richmond, Virginia.[2]: ix  The aircraft experienced two episodes of rudder reversal while on approach to land in Richmond. Unlike the two prior incidents, the rudder issues on Flight 517 spontaneously resolved and the pilots were able to safely land the aircraft. One of the 53 people on board was injured.[3]: 51 

The NTSB investigated the Eastwind incident, and incorporated information from both United Flight 585 and Eastwind Flight 517 into its ongoing investigation of the Flight 427 crash.[3]: 44 

Renewed investigation and conclusions

Because Eastwind Flight 517 had landed safely and the pilots of Flight 517 had survived, the NTSB was also able to perform tests on a plane that had experienced problems similar to the accident aircraft, was able to interview them, and gain additional information on their experience. The captain told the NTSB in a post-accident interview that they had not encountered any turbulence during the flight, and that, during their landing descent, he felt the rudder "kick" or "bump" even though neither pilot had moved the rudder pedals.[3]: 51  When the plane abruptly rolled to the right, the captain applied left aileron and attempted to move the rudder, but the rudder pedal controls felt stiffer than normal and did not seem to respond to his input; when his flight control inputs did not immediately resolve the roll upset, he also advanced the throttle of the right engine in an effort to compensate.[3]: 51–52 

The NTSB and Boeing engineers conducted a series of tests on the PCUs from Flight 517 and Flight 427, as well as PCUs used in other aircraft and a brand-new PCU that had not yet been used in flight (the PCU from Flight 585, although it had been recovered, was too badly damaged to test in this manner).[3]: 71, 81–85  Testing revealed that under certain circumstances, the PCU's dual servo valve could jam and deflect the rudder in the opposite direction of the pilots' input.[3]: 81–85  Thermal shock testing revealed that the uncommanded rudder movement could be replicated by injecting a cold PCU with hot hydraulic fluid. Thermal shock resulted in the servo's secondary slide becoming jammed against the servo housing, and that when the secondary slide was jammed the primary slide could move to a position that resulted in rudder movement opposite of the pilot's commands.[2]: 79 [3]: 294  The NTSB concluded that all three rudder incidents (United Flight 585, USAir Flight 427, and Eastwind Flight 517) were most likely due to the PCU secondary slide jamming and excessive travel of the primary slide, resulting in the rudder reversal.[3]: 294 

On March 24, 1999, after a four-year investigation, the NTSB issued its probable cause finding for Flight 427. The NTSB concluded that the probable cause of the Flight 427 crash was rudder reversal due to the PCU servo malfunction.[3]: 295  Two years later, the NTSB published an amended accident report for Flight 585 that found the same probable cause for that accident as well.

As a result of the NTSB's findings, the Federal Aviation Administration ordered that the servo valves be replaced on all 737s by November 12, 2002.[8] The FAA also ordered new training protocols for pilots to handle in an unexpected movement of flight controls.

Other suspected 737 rudder PCU malfunctions

The following Boeing 737 aircraft incidents were also suspected of being caused by a rudder PCU malfunction:

  • On June 6, 1992, Copa Airlines Flight 201, a 737-200 Advanced, flipped and crashed into the Darién Gap jungle, killing 47 people. Investigators initially believed that the airplane experienced a rudder malfunction, but after an exhaustive and extensive inquiry, they concluded that the crash was caused by faulty attitude indicator instrument readings.
  • On March 8, 1994, a Sahara Airlines aircraft that had three trainees and one supervising pilot on board crashed after performing a "touch-and-go landing" at New Delhi Airport and slammed into a Russian jet. The four pilots and five ground workers (a total of nine) were killed. Although repairs were done to the PCU with unauthorized parts, the incident is still thought to be in part due to the plane's rudder reversing both right and left.[9][10][11]
  • On April 11, 1994, a Continental Airlines pilot, Ray Miller, reported his aircraft rolled violently to the right and continued to pull to the right for another 18 minutes; the Boeing 737-300 landed safely. Continental removed the flight data recorder and rudder PCU from the incident aircraft and provided them to Boeing for investigation. Boeing concluded that the rudder had inadvertently moved due to an electrical malfunction, but only 2.5 degrees and for less than two minutes in total, a finding disputed by Miller.[9]
  • On February 23, 1999, MetroJet Flight 2710, a 737-200, experienced a slow deflection of the rudder to its blowdown limit while flying at 33,000 feet above Salisbury, Maryland. While a rudder malfunction was suspected, the aircraft was an older 737 and its flight data recorder only recorded 11 flight parameters, compared to the hundreds of parameters recorded by newer aircraft. NTSB chairman Jim Hall said that the investigation was "hampered by the lack of basic aircraft data."[12][13] All 112 passengers and five crew members (117 total) survived the incident.

SilkAir crash

On December 19, 1997, SilkAir Flight 185 crashed in Indonesia, killing 104 people. Because the crash involved a Boeing 737-300 rolling and diving toward the ground at a steep angle, investigators considered the possibility of rudder hardover due to PCU servo malfunction.[14] The Indonesian National Transportation Safety Committee, the lead investigating agency, concluded in its December 14, 2000 final report that it had found "no evidence to explain the cause of the accident."[15]: 24  However, on the same day the U.S. NTSB, which also participated in the investigation, issued its own final report that contradicted the Indonesian NTSC findings.[15]: 24–25  The NTSB's report found that there was sufficient evidence to rule out mechanical failure (based on NTSB/Parker-Hannifin's own examinations of the suspected PCU/dual-servo unit recovered from the SilkAir crash), and that the probable cause of the accident was "intentional pilot action," most likely the captain, purposely crashing the aircraft by applying sustained nose-down control pressure.[15]: 24–25 [16]

In 2004, following an independent investigation of the recovered PCU/dual-servo unit, a Los Angeles jury, which was not allowed to hear or consider the NTSB's conclusions about the accident, ruled that the 737's rudder was the cause of the crash, and ordered Parker Hannifin, the PCU/dual-servo component manufacturer, to pay US$44 million to the plaintiff families.[17] Parker Hannifin subsequently appealed the verdict, which resulted in an out-of-court settlement for an undisclosed amount.

In popular culture

The Discovery Channel Canada TV Series Mayday (called Air Crash Investigation or Air Disasters in some markets) dramatized the NTSB's 737 rudder investigation in a 2007 episode titled "Hidden Danger" (broadcast in some countries as "Mystery Crashes").[5]

Mayday separately dramatized the SilkAir crash investigation and lawsuit, including its connection to the 737 rudder controversy, in a 2012 episode titled "Pushed to the Limit" (broadcast in some countries as "Pilot Under Pressure").[14]

See also

References

  1. ^ "Report says Boeing 737 rudder problems linger". TimesDaily. September 12, 1999. Retrieved July 10, 2016.
  2. ^ a b c d e f g h i j k Uncontrolled Descent and Collision With Terrain, United Airlines Flight 585, Boeing 737-200, N999UA, 4 Miles South of Colorado Springs Municipal Airport, Colorado Springs, Colorado, March 3, 1991 (PDF). National Transportation Safety Board. March 27, 2001. NTSB/AAR-01-01. Retrieved January 17, 2016.
  3. ^ a b c d e f g h i j k l m n o p q r s Aircraft Accident Report - Uncontrolled Descent and Collision With Terrain, USAir Flight 427, Boeing 737-300, N513AU, Near Aliquippa, Pennsylvania, September 8, 1994 (PDF). National Transportation Safety Board. March 24, 1999. NTSB/AAR-99-01. Retrieved July 10, 2016.
  4. ^ "Fatal Flaws". Why Planes Crash. Season 2. 2016. MSNBC.
  5. ^ a b "Hidden Danger". Mayday. Season 4. 2007. Discovery Channel Canada / National Geographic Channel.
  6. ^ a b Equinox - "The Box", Channel 4, 2001.
  7. ^ The quick access recorder had been pioneered by BA's predecessor airline, BEA, on its Hawker Siddeley Trident aircraft back in the 1960s. Subsequently, QARs were fitted to all BEA, and then BA, aircraft.
  8. ^ . www1.airweb.faa.gov. Archived from the original on October 7, 2018. Retrieved May 21, 2016.
  9. ^ a b . The Seattle Times. October 28, 1996. Archived from the original on August 8, 2019. Retrieved May 21, 2016.
  10. ^ "ASN Aircraft accident Boeing 737-2R4C VT-SIA Delhi-Indira Gandhi International Airport (DEL)". Aviation Safety Network. Flight Safety Foundation. Retrieved May 21, 2016.
  11. ^ "Accident to Sahara India Airlines B-737-200 Aircraft During the Training Flight on 8.3.1994 at IGI Airport, Delhi Report of the Court of Inquiry". Court of Inquiry, High Court of Delhi. March 22, 1995. Retrieved May 25, 2020.
  12. ^ NTSB Office of Public Affairs (February 24, 1999). "Metrojet B-737 In-flight Event - February 23, 1999" (Press release). National Transportation Safety Board. Retrieved May 21, 2016.
  13. ^ Phillips, Don (February 26, 1999). "Aging Data Recorder Impedes Jet Probe". The Washington Post. Retrieved May 21, 2016.
  14. ^ a b "Pushed to the Limit". Mayday. Season 12. 2012. Discovery Channel Canada / National Geographic Channel.
  15. ^ a b c (PDF). Civil Aviation Safety Authority. January–February 2008. Archived from the original (PDF) on June 3, 2016. Retrieved May 21, 2016.
  16. ^ "ASN Aircraft accident Boeing 737-36N 9V-TRF Palembang". Aviation Safety Network. Flight Safety Foundation. Retrieved May 21, 2016.
  17. ^ "$43.6 Million Awarded in Silk Air Crash Cases" (PDF). www.malaysianflightmh370lawyer.com. August 17, 2004. Retrieved May 21, 2016.

External links

boeing, rudder, issues, during, 1990s, series, issues, affecting, rudder, boeing, passenger, aircraft, resulted, multiple, incidents, separate, accidents, pilots, lost, control, their, aircraft, sudden, unexpected, rudder, movement, resulting, crashes, killed,. During the 1990s a series of issues affecting the rudder of Boeing 737 passenger aircraft resulted in multiple incidents In two separate accidents pilots lost control of their aircraft due to a sudden and unexpected rudder movement and the resulting crashes killed everyone on board 157 people in total 1 Similar rudder issues led to a temporary loss of control on at least one other Boeing 737 flight before the cause of the problem was ultimately identified The National Transportation Safety Board determined that the incidents were the result of a design flaw that could result in an uncommanded movement of the aircraft s rudder 2 13 3 ix The issues were resolved after the Federal Aviation Administration ordered modifications for all Boeing 737 aircraft in service In 2016 former NTSB investigator John Cox stated that time has proven the NTSB correct in its findings because no additional rudder reversal incidents have occurred since Boeing s redesign 4 Contents 1 Rudder function 2 First accident and investigation 3 Second accident 4 Eastwind incident 5 Renewed investigation and conclusions 6 Other suspected 737 rudder PCU malfunctions 7 SilkAir crash 8 In popular culture 9 See also 10 References 11 External linksRudder function EditUnlike other twin engine large transport aircraft in service at the time the Boeing 737 was designed with a single rudder panel and single rudder actuator 2 14 The single rudder panel is controlled by a single hydraulic Power Control Unit PCU 2 13 Inside the PCU is a dual servo valve that based on input from the pilot s rudder pedals or the aircraft s yaw damper system directs the flow of hydraulic fluid in order to move the rudder 2 19 The PCU for affected Boeing 737 aircraft was designed by Boeing and manufactured by Parker Hannifin 2 20 First accident and investigation EditMain article United Airlines Flight 585 On March 3 1991 United Airlines Flight 585 a Boeing 737 200 crashed while attempting to land in Colorado Springs Colorado During the airplane s landing approach the plane rolled to the right and pitched nose down into a near vertical dive 2 ix The resulting crash destroyed the aircraft and killed all 25 people on board 2 ix Although the NTSB investigated the accident it was unable to conclusively identify the cause of the crash The rudder PCU from Flight 585 was severely damaged which prevented operational testing of the PCU 3 47 A review of the flight crew s history determined that Flight 585 s captain strictly adhered to operating procedures and had a conservative approach to flying 3 47 A first officer who had previously flown with Flight 585 s captain reported that the captain had indicated to him while landing in turbulent weather that the captain had no problem with declaring a go around if the landing appeared unsafe 3 48 The first officer was considered to be very competent by the captain on previous trips they had flown together 3 48 The weather data available to the NTSB indicated that Flight 585 might have encountered a horizontal axis wind vortex that could have caused the aircraft to roll over but this could not be shown conclusively to have happened or to have caused the rollover 3 48 49 On December 8 1992 the NTSB published a report that identified what the NTSB believed at the time to be the two most likely causes of the accident The first possibility was that the airplane s directional control system had malfunctioned and caused the rudder to move in a manner that caused the accident The second possibility was a weather disturbance that caused a sudden rudder movement or loss of control The Board determined that it lacked sufficient evidence to conclude either theory as the probable cause of the accident 2 ix 3 49 This was only the fourth time in the NTSB s history that it had closed an investigation and published a final aircraft accident report where the probable cause was undetermined 5 Second accident EditMain article USAir Flight 427 On September 8 1994 USAir Flight 427 a Boeing 737 300 crashed near Pittsburgh Pennsylvania While on approach to Pittsburgh International Airport Flight 427 suddenly rolled to the left Although the pilots were briefly able to roll right and level the plane it rolled left a second time and the pilots were unable to recover 3 4 The resulting crash killed all 132 people on board 3 9 The NTSB realized early into its investigation that the crash of Flight 427 might have been caused by an unintended or uncommanded rudder movement similar to the suspected but not yet established cause of the Flight 585 crash 3 44 As a result the NTSB conducted additional testing on United Flight 585 s Parker Hannifin PCU servo during its Flight 427 investigation 2 73 One of the problems facing investigators was the relative lack of precision in the data produced by the flight data recorder FDR which only recorded control inputs at periodic intervals with significant time gaps between samples gaps during which no data was recorded no matter what the pilot did with the controls This lack of precision led to it being possible for Boeing to interpret the data differently from the way the NTSB did leading the manufacturer to suspect and insist that the pilot had responded incorrectly to a wake turbulence incident 6 At the request of the NTSB data from the Penny amp Giles quick access recorder QAR of a British Airways BA Boeing 747 400 was supplied to the NTSB by BA The data was from a London Bangkok flight in which the aircraft suffered an uncommanded elevator movement and momentary elevator reversal on take off the aircraft then landed safely Operating alongside the FDR system the QAR on BA s 747 400s in conjunction with a Data Management Unit received and recorded more aircraft parametric data including control input values at a higher rate 7 This BA data led to renewed suspicion of the similar valve design used on the 737 rudder As a result of this earlier BA incident Boeing had in fact modified the design of the 747 elevator servo system and the modified system had been retroactively fitted to all 747 400s in service 6 Eastwind incident EditMain article Eastwind Airlines Flight 517 On June 9 1996 while the NTSB s investigation of Flight 427 was still ongoing the pilots of Eastwind Airlines Flight 517 briefly lost control of their aircraft a 737 200 while flying from Trenton New Jersey to Richmond Virginia 2 ix The aircraft experienced two episodes of rudder reversal while on approach to land in Richmond Unlike the two prior incidents the rudder issues on Flight 517 spontaneously resolved and the pilots were able to safely land the aircraft One of the 53 people on board was injured 3 51 The NTSB investigated the Eastwind incident and incorporated information from both United Flight 585 and Eastwind Flight 517 into its ongoing investigation of the Flight 427 crash 3 44 Renewed investigation and conclusions EditBecause Eastwind Flight 517 had landed safely and the pilots of Flight 517 had survived the NTSB was also able to perform tests on a plane that had experienced problems similar to the accident aircraft was able to interview them and gain additional information on their experience The captain told the NTSB in a post accident interview that they had not encountered any turbulence during the flight and that during their landing descent he felt the rudder kick or bump even though neither pilot had moved the rudder pedals 3 51 When the plane abruptly rolled to the right the captain applied left aileron and attempted to move the rudder but the rudder pedal controls felt stiffer than normal and did not seem to respond to his input when his flight control inputs did not immediately resolve the roll upset he also advanced the throttle of the right engine in an effort to compensate 3 51 52 The NTSB and Boeing engineers conducted a series of tests on the PCUs from Flight 517 and Flight 427 as well as PCUs used in other aircraft and a brand new PCU that had not yet been used in flight the PCU from Flight 585 although it had been recovered was too badly damaged to test in this manner 3 71 81 85 Testing revealed that under certain circumstances the PCU s dual servo valve could jam and deflect the rudder in the opposite direction of the pilots input 3 81 85 Thermal shock testing revealed that the uncommanded rudder movement could be replicated by injecting a cold PCU with hot hydraulic fluid Thermal shock resulted in the servo s secondary slide becoming jammed against the servo housing and that when the secondary slide was jammed the primary slide could move to a position that resulted in rudder movement opposite of the pilot s commands 2 79 3 294 The NTSB concluded that all three rudder incidents United Flight 585 USAir Flight 427 and Eastwind Flight 517 were most likely due to the PCU secondary slide jamming and excessive travel of the primary slide resulting in the rudder reversal 3 294 On March 24 1999 after a four year investigation the NTSB issued its probable cause finding for Flight 427 The NTSB concluded that the probable cause of the Flight 427 crash was rudder reversal due to the PCU servo malfunction 3 295 Two years later the NTSB published an amended accident report for Flight 585 that found the same probable cause for that accident as well As a result of the NTSB s findings the Federal Aviation Administration ordered that the servo valves be replaced on all 737s by November 12 2002 8 The FAA also ordered new training protocols for pilots to handle in an unexpected movement of flight controls Other suspected 737 rudder PCU malfunctions EditThe following Boeing 737 aircraft incidents were also suspected of being caused by a rudder PCU malfunction On June 6 1992 Copa Airlines Flight 201 a 737 200 Advanced flipped and crashed into the Darien Gap jungle killing 47 people Investigators initially believed that the airplane experienced a rudder malfunction but after an exhaustive and extensive inquiry they concluded that the crash was caused by faulty attitude indicator instrument readings On March 8 1994 a Sahara Airlines aircraft that had three trainees and one supervising pilot on board crashed after performing a touch and go landing at New Delhi Airport and slammed into a Russian jet The four pilots and five ground workers a total of nine were killed Although repairs were done to the PCU with unauthorized parts the incident is still thought to be in part due to the plane s rudder reversing both right and left 9 10 11 On April 11 1994 a Continental Airlines pilot Ray Miller reported his aircraft rolled violently to the right and continued to pull to the right for another 18 minutes the Boeing 737 300 landed safely Continental removed the flight data recorder and rudder PCU from the incident aircraft and provided them to Boeing for investigation Boeing concluded that the rudder had inadvertently moved due to an electrical malfunction but only 2 5 degrees and for less than two minutes in total a finding disputed by Miller 9 On February 23 1999 MetroJet Flight 2710 a 737 200 experienced a slow deflection of the rudder to its blowdown limit while flying at 33 000 feet above Salisbury Maryland While a rudder malfunction was suspected the aircraft was an older 737 and its flight data recorder only recorded 11 flight parameters compared to the hundreds of parameters recorded by newer aircraft NTSB chairman Jim Hall said that the investigation was hampered by the lack of basic aircraft data 12 13 All 112 passengers and five crew members 117 total survived the incident SilkAir crash EditMain article SilkAir Flight 185 On December 19 1997 SilkAir Flight 185 crashed in Indonesia killing 104 people Because the crash involved a Boeing 737 300 rolling and diving toward the ground at a steep angle investigators considered the possibility of rudder hardover due to PCU servo malfunction 14 The Indonesian National Transportation Safety Committee the lead investigating agency concluded in its December 14 2000 final report that it had found no evidence to explain the cause of the accident 15 24 However on the same day the U S NTSB which also participated in the investigation issued its own final report that contradicted the Indonesian NTSC findings 15 24 25 The NTSB s report found that there was sufficient evidence to rule out mechanical failure based on NTSB Parker Hannifin s own examinations of the suspected PCU dual servo unit recovered from the SilkAir crash and that the probable cause of the accident was intentional pilot action most likely the captain purposely crashing the aircraft by applying sustained nose down control pressure 15 24 25 16 In 2004 following an independent investigation of the recovered PCU dual servo unit a Los Angeles jury which was not allowed to hear or consider the NTSB s conclusions about the accident ruled that the 737 s rudder was the cause of the crash and ordered Parker Hannifin the PCU dual servo component manufacturer to pay US 44 million to the plaintiff families 17 Parker Hannifin subsequently appealed the verdict which resulted in an out of court settlement for an undisclosed amount In popular culture EditThe Discovery Channel Canada TV Series Mayday called Air Crash Investigation or Air Disasters in some markets dramatized the NTSB s 737 rudder investigation in a 2007 episode titled Hidden Danger broadcast in some countries as Mystery Crashes 5 Mayday separately dramatized the SilkAir crash investigation and lawsuit including its connection to the 737 rudder controversy in a 2012 episode titled Pushed to the Limit broadcast in some countries as Pilot Under Pressure 14 See also EditBoeing 737 MAX groundings aircraft issues involving the latest variants of Boeing 737 Northwest Airlines Flight 85 rudder hardover event involving a 747 400 Continental Airlines Flight 1404 a Boeing 737 that exited the left side of the runway and caught fireReferences Edit Report says Boeing 737 rudder problems linger TimesDaily September 12 1999 Retrieved July 10 2016 a b c d e f g h i j k Uncontrolled Descent and Collision With Terrain United Airlines Flight 585 Boeing 737 200 N999UA 4 Miles South of Colorado Springs Municipal Airport Colorado Springs Colorado March 3 1991 PDF National Transportation Safety Board March 27 2001 NTSB AAR 01 01 Retrieved January 17 2016 a b c d e f g h i j k l m n o p q r s Aircraft Accident Report Uncontrolled Descent and Collision With Terrain USAir Flight 427 Boeing 737 300 N513AU Near Aliquippa Pennsylvania September 8 1994 PDF National Transportation Safety Board March 24 1999 NTSB AAR 99 01 Retrieved July 10 2016 Fatal Flaws Why Planes Crash Season 2 2016 MSNBC a b Hidden Danger Mayday Season 4 2007 Discovery Channel Canada National Geographic Channel a b Equinox The Box Channel 4 2001 The quick access recorder had been pioneered by BA s predecessor airline BEA on its Hawker Siddeley Trident aircraft back in the 1960s Subsequently QARs were fitted to all BEA and then BA aircraft Boeing Model 737 Series Airplanes www1 airweb faa gov Archived from the original on October 7 2018 Retrieved May 21 2016 a b 737 The crash in Colorado Springs The Seattle Times October 28 1996 Archived from the original on August 8 2019 Retrieved May 21 2016 ASN Aircraft accident Boeing 737 2R4C VT SIA Delhi Indira Gandhi International Airport DEL Aviation Safety Network Flight Safety Foundation Retrieved May 21 2016 Accident to Sahara India Airlines B 737 200 Aircraft During the Training Flight on 8 3 1994 at IGI Airport Delhi Report of the Court of Inquiry Court of Inquiry High Court of Delhi March 22 1995 Retrieved May 25 2020 NTSB Office of Public Affairs February 24 1999 Metrojet B 737 In flight Event February 23 1999 Press release National Transportation Safety Board Retrieved May 21 2016 Phillips Don February 26 1999 Aging Data Recorder Impedes Jet Probe The Washington Post Retrieved May 21 2016 a b Pushed to the Limit Mayday Season 12 2012 Discovery Channel Canada National Geographic Channel a b c Final Flight SilkAir PDF Civil Aviation Safety Authority January February 2008 Archived from the original PDF on June 3 2016 Retrieved May 21 2016 ASN Aircraft accident Boeing 737 36N 9V TRF Palembang Aviation Safety Network Flight Safety Foundation Retrieved May 21 2016 43 6 Million Awarded in Silk Air Crash Cases PDF www malaysianflightmh370lawyer com August 17 2004 Retrieved May 21 2016 External links Edit Aviation portal 1990s portalHow the 737 rudder works Boeing 737 Rudder Design Study Archived July 29 2012 at the Wayback Machine Retrieved from https en wikipedia org w index php title Boeing 737 rudder issues amp oldid 1126857675, wikipedia, wiki, book, books, library,

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