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Southwest Airlines Flight 1455

Southwest Airlines Flight 1455 was a scheduled passenger flight from McCarran International Airport, Las Vegas, Nevada, to Burbank-Glendale-Pasadena Airport, Burbank, California, that overran the runway during landing on March 5, 2000. The aircraft, a Boeing 737-3T5, registration N668SW,[2] came to rest on a city street adjacent to a gas station. The National Transportation Safety Board found that the incident was due to the pilots attempting to land with excessive speed. They also found that the air traffic controller placed them in a position from which their only option was a go around. Two of the passengers were seriously injured, and there were many minor injuries. As a result of the incident, the airport installed an Engineered Materials Arrestor System (EMAS) at the east end of the incident runway. The aircraft was written off, making the incident the 10th hull loss of a Boeing 737-300.[1] This was the first major accident in the airline's 29-year history.[3]

Southwest Airlines Flight 1455
N668SW, following its runway overrun at Hollywood Burbank Bob Hope Airport.
Accident
DateMarch 5, 2000 (2000-03-05)
SummaryRunway overrun due to pilot error and ATC error[1]
SiteHollywood Burbank Bob Hope Airport,
Burbank, California
34°11′50″N 118°20′56″W / 34.19722°N 118.34889°W / 34.19722; -118.34889
Aircraft
Aircraft typeBoeing 737-3T5
OperatorSouthwest Airlines
IATA flight No.WN1455
ICAO flight No.SWA1455
Call signSOUTHWEST 1455
RegistrationN668SW
Flight originMcCarran International Airport, Las Vegas, Nevada
DestinationBurbank-Glendale-Pasadena Airport, Burbank, California
Occupants142
Passengers137
Crew5
Fatalities0
Injuries44
Survivors142

Aircraft and crew edit

 
The aircraft involved in 1991, while still in service with Britannia Airways.

The aircraft was a 15 year old Boeing 737-3T5 (registration N668SW[4]). The 737 was one of the oldest aircraft in Southwest's fleet, having been originally built for Orion Airways in 1984. The aircraft was powered by two CFM International CFM56-3B1 turbofan engines.[5]: 7–8 

The captain was 52-year-old Howard Peterson, who had been with Southwest Airlines since 1988 and had logged 11,000 flight hours, including 9,870 hours on the Boeing 737. The first officer was 43-year-old Jeffrey D. Erwin, who had been with Southwest Airlines since 1995 and had 5,032 flight hours, with 2,522 of them on the Boeing 737.[5]: 5–7 

Peterson served as a pilot in the U.S. Air Force from 1970 to 1975, then flew for United Airlines from 1975 to 1977, and then flew for Wien Air Alaska from 1977 to 1979, and also flew for Coleman Air Transport from 1979 to 1980, before flying for EG&G from 1980 to 1988. Erwin also served as a pilot in the U.S. Air Force from 1983 to 1995.

Accident edit

Flight 1455 departed McCarran International Airport (LAS), Las Vegas, Nevada, at 1650, more than 2 hours behind schedule due to inclement weather in the area. At 18:04:02, when the aircraft was 19 nautical miles (22 mi; 35 km) north of the BUR outer marker, the SoCal approach controller instructed the aircraft to maintain 230 knots (260 mph; 430 km/h) or greater until further notice. The controller later informed the captain to place the aircraft into the approach pattern between two other flights. The captain acknowledged the instructions.

At 18:04:42 the first officer informed the captain that the target airspeed for landing would be 138 knots (159 mph; 256 km/h). This value was based on standard procedures in the Southwest Airlines Flight Operations Manual (FOM). At 18:05:13 the captain told the first officer that the air traffic controller had instructed them to remain at 230 knots (260 mph; 430 km/h) or greater "for a while."

At 18:05:54 the controller cleared Flight 1455 to descend to 5,000 feet (1,500 m), and at 1807 cleared the flight to descend to 3,000 feet (900 m). At 1808 the controller cleared flight 1455 for a visual approach to runway 8 with a restriction to remain at or above 3,000 feet (above mean sea level) until passing the Van Nuys VOR beacon. This navigational aid is approximately 6 miles (5 nmi; 10 km) from the runway. Radar data suggest that the flight began its descent from 3,000 feet (910 m) about 4 miles (3 nmi; 6 km) from the runway.[6]

According to the Aeronautical Information Manual Section 4-4-12f,[7] this approach clearance automatically canceled any previous speed assignments. According to the final accident report, traffic conditions no longer warranted the speed assignment after the controller cleared the flight to descend to 3,000 feet (910 m), but the controller did not verbally cancel the speed assignment.

Southwest Airlines procedures then in place had the non-flying pilot (pilot monitoring) make altitude call-outs at 1000, 500, 400, 300, 200, 100, 50, 30, and 10 feet (3.0 m). Additionally, call-outs are required if certain parameters are not met, in this case flight speed and sink rate. At 1809:32, one minute and thirteen seconds after approach clearance was given, and at 3,000 feet (910 m) of altitude, the captain began to slow the aircraft by deploying the flaps.

At 18:10:24 the ground proximity warning system (GPWS) began to sound a "sink rate" warning in the cockpit. The aircraft was descending at an angle of 7 degrees, when the angle of descent for most aircraft landing on that runway was 3 or 4 degrees. Both pilots ignored the warnings. At 18:10:44 the warning system in the cockpit began to sound. The captain responded to these warnings with "that's all right."

The captain stated after the accident that he knew as the aircraft passed 500 feet (150 m) that he was not "in the slot," meaning the conditions had not been met for a safe landing, in this case because of an excessive airspeed. The captain further stated that he understood that if he was not "in the slot," procedures demanded a go-around maneuver to abort the landing. He could not explain why he did not perform a go-around maneuver. The first officer likewise indicated after the accident that he was aware that they were not "in the slot," but said he believed the captain was taking corrective action.

The aircraft touched down on the wet runway at 44 knots (51 mph; 81 km/h) over the target airspeed. Furthermore, it touched down 2,150 feet (660 m) from the runway threshold, 650 feet (200 m) beyond the 1,000–1,500-foot (300–460 m) range established by the Southwest Airlines FOM. The captain deployed the thrust reversers and then he and the first officer applied manual brakes, but according to later NTSB findings, under those conditions even maximum braking would not have prevented the aircraft from overrunning the end of the runway.

Unable to stop in time, the Boeing 737 overran the end of Runway 8. "The airplane touched down at approximately 182 knots (209 mph; 337 km/h), and about 20 seconds later, at approximately 32 knots (37 mph; 59 km/h), collided with a metal blast fence and an airport perimeter wall."[5] It finally came to rest on Hollywood Way, a four-lane city street, near a Chevron gas station. The nose section and front landing gear were sheared off, but otherwise the fuselage remained intact and there was no compromise of the cabin area. However, the 737 sustained structural damage from the accident and was later scrapped.

The cockpit voice recorder captured the flight's captain remarking, "Well, there goes my career," moments after the accident.[8]

Investigation edit

The NTSB concluded that the probable cause for the accident was excessive flight speed and the steep angle of the glidepath (7 degrees, as opposed to the 3 degrees normally used for both visual and instrument approaches), and the flight crew's failure to abort the approach when conditions were not met for a stable approach and landing. The action of the flight controller was listed as a contributing factor in the accident: "Contributing to the accident was the controller's positioning of the airplane in such a manner as to leave no safe options for the flight crew other than a go-around maneuver."[5]

Months later, the pilots were fired as a result of this incident.[9] Southwest Airlines admitted the pilots' actions were negligent.[10]

At the time, a Southwest spokesperson termed it "the worst accident" in the airline's history.[11][12] Air safety experts and pilots suggested the accident was an example of a situation where "fast, steep, unstabilized approaches" are dangerous, and of how inadequate the safety margins around the Burbank runways are (as well as similar U.S. airports).[13]

The gas station missed by the aircraft was later closed and demolished due to safety concerns. The lot became dedicated green space.

Injuries edit

Of the 142 people on board, 2 passengers sustained serious injuries; 41 passengers and the captain sustained minor injuries; and 94 passengers, 3 flight attendants, and the first officer sustained no injuries. The airplane sustained extensive exterior damage and some internal damage to the passenger cabin.

The 737 struck a vehicle on Hollywood Way, pinning the vehicle's hood under the aircraft. However, the vehicle's two occupants (the driver and her four-year-old daughter) were not injured. No other ground injuries were reported.[14]

During the accident sequence, the forward service door (1R) escape slide inflated inside the airplane; the nose gear collapsed; and the forward dual flight attendant jumpseat, which was occupied by two flight attendants, partially collapsed.

The inflated escape slide blocked both forward doors from being used to evacuate the aircraft, and prevented two flight attendants seated on the forward jumpseat from assisting the evacuation. There was no fire, but had there been a fire, this malfunctioning slide would have dramatically affected the survivability of the occupants. As a result of this occurrence, the NTSB issued a safety recommendation to replace the slide cover latch brackets on forward slide compartments of all older Boeing 737 models with the latch brackets installed on later models.

Subsequent safety measures edit

As with runway 4R/22L at the Little Rock National Airport, site of the American Airlines Flight 1420 overrun accident, runway 8/26 in Burbank was exempt from the 1,000-foot (300 m) runway safety area standard. The NTSB cited this accident in a recommendation for installing the engineered materials arrestor system (EMAS) at airports where it is not feasible to establish the 1,000-foot (300 m) runway safety area (RSA).[15] A US $4,000,000 EMAS was subsequently installed as a result of this accident at Burbank airport.

On Friday, October 13, 2006, the Burbank EMAS stopped a private jet with no injuries or aircraft damage.

On December 6, 2018, it stopped a Southwest 737-700 (N752SW), with 117 people on board. There were no injuries and no damage to the aircraft.[16]

Dispute with city of Burbank edit

Burbank city officials demanded that Southwest Airlines pay their $40,000 bill for services, including overtime for police officers and firefighters, related to the March 5, 2000, accident. Southwest refused to pay stating that the airline is entitled to emergency services since it pays taxes to the city.[17]

See also edit

References edit

  1. ^ a b Ranter, Harro. "ASN Aircraft accident Boeing 737-3T5 N668SW Burbank/Glendale/Pasadena Airport, CA (BUR)". aviation-safety.net. Retrieved January 13, 2019.
  2. ^ "FAA Registry (N668SW)". Federal Aviation Administration.
  3. ^ Pringle, Paul; Lunsford, J. Lynn (March 6, 2000). "Southwest Airlines jet skids onto busy California street - Injuries minor as place hits fence, stops near gas station". The Dallas Morning News. Dallas, Texas.
  4. ^ "FAA Registry (N668SW)". Federal Aviation Administration.
  5. ^ a b c d "Southwest Airlines flight 1455, Burbank, California, March 5, 2000" (PDF). National Transportation Safety Board. June 26, 2002. NTSB/AAB-02/04. Retrieved January 13, 2015.
  6. ^ "Statement By Chairman Jim Hall on the NTSB Investigation of the Runway Overrun Accident Involving Southwest Airlines Flight 1455". National Transportation Safety Board. March 7, 2000. Retrieved June 16, 2007.
  7. ^ AIM Section 4-4-12f January 25, 2010, at the Wayback MachineFAA AIM 02-14-2008 incl. Changes 1-3 July 12, 2009, at the Wayback Machine
  8. ^ "'My Fault,' Pilot Admits in Burbank Jet Mishap". Los Angeles Daily News. July 11, 2001. 'Well, there goes my career.'
  9. ^ "Southwest Fires Pilots for Burbank Crash Landing". ABC News. Retrieved March 11, 2016.
  10. ^ "Southwest Concedes Pilot Negligence". AP News. Associated Press. October 8, 2001. Southwest Airlines is willing to concede its fired pilots were negligent when a jet skidded off a runway and onto a street during a botched landing at Hollywood Burbank Bob Hope Airport last year, the airline's attorney said.
  11. ^ Lunsford, J. Lynn (August 2, 2000). "Southwest Airlines Fires Pilot, Co-Pilot Involved in Burbank, Calif., Crash". Knight Ridder/Tribune Business News. The airline fired the pilots after completing an internal investigation of the March 5 crash of Flight 1455, which was the first major accident in Southwest's 29-year history.
  12. ^ "Runaway jet that narrowly missed gas station triggers talk of what-ifs". Milwaukee Journal Sentinel. Retrieved August 2, 2013.[dead link]
  13. ^ "Overrun Highlights Hazard of Unstabilized Approaches". Air Safety Week. Archived from the original on July 10, 2012. Retrieved August 2, 2013.
  14. ^ "Jetliner barrels off runway; Plane comes to stop in California street". Associated Press. March 6, 2000. Retrieved January 28, 2020.
  15. ^ (PDF). National Transportation Safety Board. December 10, 2001. Archived from the original (PDF) on September 30, 2007. Retrieved June 15, 2007.
  16. ^ Hradeky, Simon (December 6, 2018). "Incident: Southwest B737 at Burbank on Dec 6th 2018, overran runway on landing". Aviation Herald.
  17. ^ Oliande, Sylvia L. (February 22, 2001). . Los Angeles Daily News. Archived from the original on March 12, 2016. Retrieved March 11, 2016. City officials said Wednesday they will likely continue to push Southwest to pay the $40,000 bill for services, including overtime for police officers and firefighters, provided in the wake of the March 5 mishap.

External links edit

  • NTSB investigation docket

southwest, airlines, flight, 1455, scheduled, passenger, flight, from, mccarran, international, airport, vegas, nevada, burbank, glendale, pasadena, airport, burbank, california, that, overran, runway, during, landing, march, 2000, aircraft, boeing, registrati. Southwest Airlines Flight 1455 was a scheduled passenger flight from McCarran International Airport Las Vegas Nevada to Burbank Glendale Pasadena Airport Burbank California that overran the runway during landing on March 5 2000 The aircraft a Boeing 737 3T5 registration N668SW 2 came to rest on a city street adjacent to a gas station The National Transportation Safety Board found that the incident was due to the pilots attempting to land with excessive speed They also found that the air traffic controller placed them in a position from which their only option was a go around Two of the passengers were seriously injured and there were many minor injuries As a result of the incident the airport installed an Engineered Materials Arrestor System EMAS at the east end of the incident runway The aircraft was written off making the incident the 10th hull loss of a Boeing 737 300 1 This was the first major accident in the airline s 29 year history 3 Southwest Airlines Flight 1455N668SW following its runway overrun at Hollywood Burbank Bob Hope Airport AccidentDateMarch 5 2000 2000 03 05 SummaryRunway overrun due to pilot error and ATC error 1 SiteHollywood Burbank Bob Hope Airport Burbank California 34 11 50 N 118 20 56 W 34 19722 N 118 34889 W 34 19722 118 34889AircraftAircraft typeBoeing 737 3T5OperatorSouthwest AirlinesIATA flight No WN1455ICAO flight No SWA1455Call signSOUTHWEST 1455RegistrationN668SWFlight originMcCarran International Airport Las Vegas NevadaDestinationBurbank Glendale Pasadena Airport Burbank CaliforniaOccupants142Passengers137Crew5Fatalities0Injuries44Survivors142 Contents 1 Aircraft and crew 2 Accident 3 Investigation 4 Injuries 5 Subsequent safety measures 6 Dispute with city of Burbank 7 See also 8 References 9 External linksAircraft and crew edit nbsp The aircraft involved in 1991 while still in service with Britannia Airways The aircraft was a 15 year old Boeing 737 3T5 registration N668SW 4 The 737 was one of the oldest aircraft in Southwest s fleet having been originally built for Orion Airways in 1984 The aircraft was powered by two CFM International CFM56 3B1 turbofan engines 5 7 8 The captain was 52 year old Howard Peterson who had been with Southwest Airlines since 1988 and had logged 11 000 flight hours including 9 870 hours on the Boeing 737 The first officer was 43 year old Jeffrey D Erwin who had been with Southwest Airlines since 1995 and had 5 032 flight hours with 2 522 of them on the Boeing 737 5 5 7 Peterson served as a pilot in the U S Air Force from 1970 to 1975 then flew for United Airlines from 1975 to 1977 and then flew for Wien Air Alaska from 1977 to 1979 and also flew for Coleman Air Transport from 1979 to 1980 before flying for EG amp G from 1980 to 1988 Erwin also served as a pilot in the U S Air Force from 1983 to 1995 Accident editFlight 1455 departed McCarran International Airport LAS Las Vegas Nevada at 1650 more than 2 hours behind schedule due to inclement weather in the area At 18 04 02 when the aircraft was 19 nautical miles 22 mi 35 km north of the BUR outer marker the SoCal approach controller instructed the aircraft to maintain 230 knots 260 mph 430 km h or greater until further notice The controller later informed the captain to place the aircraft into the approach pattern between two other flights The captain acknowledged the instructions At 18 04 42 the first officer informed the captain that the target airspeed for landing would be 138 knots 159 mph 256 km h This value was based on standard procedures in the Southwest Airlines Flight Operations Manual FOM At 18 05 13 the captain told the first officer that the air traffic controller had instructed them to remain at 230 knots 260 mph 430 km h or greater for a while At 18 05 54 the controller cleared Flight 1455 to descend to 5 000 feet 1 500 m and at 1807 cleared the flight to descend to 3 000 feet 900 m At 1808 the controller cleared flight 1455 for a visual approach to runway 8 with a restriction to remain at or above 3 000 feet above mean sea level until passing the Van Nuys VOR beacon This navigational aid is approximately 6 miles 5 nmi 10 km from the runway Radar data suggest that the flight began its descent from 3 000 feet 910 m about 4 miles 3 nmi 6 km from the runway 6 According to the Aeronautical Information Manual Section 4 4 12f 7 this approach clearance automatically canceled any previous speed assignments According to the final accident report traffic conditions no longer warranted the speed assignment after the controller cleared the flight to descend to 3 000 feet 910 m but the controller did not verbally cancel the speed assignment Southwest Airlines procedures then in place had the non flying pilot pilot monitoring make altitude call outs at 1000 500 400 300 200 100 50 30 and 10 feet 3 0 m Additionally call outs are required if certain parameters are not met in this case flight speed and sink rate At 1809 32 one minute and thirteen seconds after approach clearance was given and at 3 000 feet 910 m of altitude the captain began to slow the aircraft by deploying the flaps At 18 10 24 the ground proximity warning system GPWS began to sound a sink rate warning in the cockpit The aircraft was descending at an angle of 7 degrees when the angle of descent for most aircraft landing on that runway was 3 or 4 degrees Both pilots ignored the warnings At 18 10 44 the warning system in the cockpit began to sound The captain responded to these warnings with that s all right The captain stated after the accident that he knew as the aircraft passed 500 feet 150 m that he was not in the slot meaning the conditions had not been met for a safe landing in this case because of an excessive airspeed The captain further stated that he understood that if he was not in the slot procedures demanded a go around maneuver to abort the landing He could not explain why he did not perform a go around maneuver The first officer likewise indicated after the accident that he was aware that they were not in the slot but said he believed the captain was taking corrective action The aircraft touched down on the wet runway at 44 knots 51 mph 81 km h over the target airspeed Furthermore it touched down 2 150 feet 660 m from the runway threshold 650 feet 200 m beyond the 1 000 1 500 foot 300 460 m range established by the Southwest Airlines FOM The captain deployed the thrust reversers and then he and the first officer applied manual brakes but according to later NTSB findings under those conditions even maximum braking would not have prevented the aircraft from overrunning the end of the runway Unable to stop in time the Boeing 737 overran the end of Runway 8 The airplane touched down at approximately 182 knots 209 mph 337 km h and about 20 seconds later at approximately 32 knots 37 mph 59 km h collided with a metal blast fence and an airport perimeter wall 5 It finally came to rest on Hollywood Way a four lane city street near a Chevron gas station The nose section and front landing gear were sheared off but otherwise the fuselage remained intact and there was no compromise of the cabin area However the 737 sustained structural damage from the accident and was later scrapped The cockpit voice recorder captured the flight s captain remarking Well there goes my career moments after the accident 8 Investigation editThe NTSB concluded that the probable cause for the accident was excessive flight speed and the steep angle of the glidepath 7 degrees as opposed to the 3 degrees normally used for both visual and instrument approaches and the flight crew s failure to abort the approach when conditions were not met for a stable approach and landing The action of the flight controller was listed as a contributing factor in the accident Contributing to the accident was the controller s positioning of the airplane in such a manner as to leave no safe options for the flight crew other than a go around maneuver 5 Months later the pilots were fired as a result of this incident 9 Southwest Airlines admitted the pilots actions were negligent 10 At the time a Southwest spokesperson termed it the worst accident in the airline s history 11 12 Air safety experts and pilots suggested the accident was an example of a situation where fast steep unstabilized approaches are dangerous and of how inadequate the safety margins around the Burbank runways are as well as similar U S airports 13 The gas station missed by the aircraft was later closed and demolished due to safety concerns The lot became dedicated green space Injuries editOf the 142 people on board 2 passengers sustained serious injuries 41 passengers and the captain sustained minor injuries and 94 passengers 3 flight attendants and the first officer sustained no injuries The airplane sustained extensive exterior damage and some internal damage to the passenger cabin The 737 struck a vehicle on Hollywood Way pinning the vehicle s hood under the aircraft However the vehicle s two occupants the driver and her four year old daughter were not injured No other ground injuries were reported 14 During the accident sequence the forward service door 1R escape slide inflated inside the airplane the nose gear collapsed and the forward dual flight attendant jumpseat which was occupied by two flight attendants partially collapsed The inflated escape slide blocked both forward doors from being used to evacuate the aircraft and prevented two flight attendants seated on the forward jumpseat from assisting the evacuation There was no fire but had there been a fire this malfunctioning slide would have dramatically affected the survivability of the occupants As a result of this occurrence the NTSB issued a safety recommendation to replace the slide cover latch brackets on forward slide compartments of all older Boeing 737 models with the latch brackets installed on later models Subsequent safety measures editAs with runway 4R 22L at the Little Rock National Airport site of the American Airlines Flight 1420 overrun accident runway 8 26 in Burbank was exempt from the 1 000 foot 300 m runway safety area standard The NTSB cited this accident in a recommendation for installing the engineered materials arrestor system EMAS at airports where it is not feasible to establish the 1 000 foot 300 m runway safety area RSA 15 A US 4 000 000 EMAS was subsequently installed as a result of this accident at Burbank airport On Friday October 13 2006 the Burbank EMAS stopped a private jet with no injuries or aircraft damage On December 6 2018 it stopped a Southwest 737 700 N752SW with 117 people on board There were no injuries and no damage to the aircraft 16 Dispute with city of Burbank editBurbank city officials demanded that Southwest Airlines pay their 40 000 bill for services including overtime for police officers and firefighters related to the March 5 2000 accident Southwest refused to pay stating that the airline is entitled to emergency services since it pays taxes to the city 17 See also edit nbsp Los Angeles portal nbsp Aviation portalEngineered materials arrestor system Ground effect aerodynamics Runway safety area Southwest Airlines Flight 1248 Chicago Midway International Airport overrun accident on December 8 2005 TAM Airlines Flight 3054 A similar runway overrun crash that occurred 7 years later where an Airbus A320 landed on a wet runway and hit a gas station killing all 187 onboard and 12 on the ground References edit a b Ranter Harro ASN Aircraft accident Boeing 737 3T5 N668SW Burbank Glendale Pasadena Airport CA BUR aviation safety net Retrieved January 13 2019 FAA Registry N668SW Federal Aviation Administration Pringle Paul Lunsford J Lynn March 6 2000 Southwest Airlines jet skids onto busy California street Injuries minor as place hits fence stops near gas station The Dallas Morning News Dallas Texas FAA Registry N668SW Federal Aviation Administration a b c d Southwest Airlines flight 1455 Burbank California March 5 2000 PDF National Transportation Safety Board June 26 2002 NTSB AAB 02 04 Retrieved January 13 2015 Statement By Chairman Jim Hall on the NTSB Investigation of the Runway Overrun Accident Involving Southwest Airlines Flight 1455 National Transportation Safety Board March 7 2000 Retrieved June 16 2007 AIM Section 4 4 12f Archived January 25 2010 at the Wayback MachineFAA AIM 02 14 2008 incl Changes 1 3 Archived July 12 2009 at the Wayback Machine My Fault Pilot Admits in Burbank Jet Mishap Los Angeles Daily News July 11 2001 Well there goes my career Southwest Fires Pilots for Burbank Crash Landing ABC News Retrieved March 11 2016 Southwest Concedes Pilot Negligence AP News Associated Press October 8 2001 Southwest Airlines is willing to concede its fired pilots were negligent when a jet skidded off a runway and onto a street during a botched landing at Hollywood Burbank Bob Hope Airport last year the airline s attorney said Lunsford J Lynn August 2 2000 Southwest Airlines Fires Pilot Co Pilot Involved in Burbank Calif Crash Knight Ridder Tribune Business News The airline fired the pilots after completing an internal investigation of the March 5 crash of Flight 1455 which was the first major accident in Southwest s 29 year history Runaway jet that narrowly missed gas station triggers talk of what ifs Milwaukee Journal Sentinel Retrieved August 2 2013 dead link Overrun Highlights Hazard of Unstabilized Approaches Air Safety Week Archived from the original on July 10 2012 Retrieved August 2 2013 Jetliner barrels off runway Plane comes to stop in California street Associated Press March 6 2000 Retrieved January 28 2020 NTSB Safety Recommendation A 01 49 through 70 PDF National Transportation Safety Board December 10 2001 Archived from the original PDF on September 30 2007 Retrieved June 15 2007 Hradeky Simon December 6 2018 Incident Southwest B737 at Burbank on Dec 6th 2018 overran runway on landing Aviation Herald Oliande Sylvia L February 22 2001 Airline Balks at Bill in Skid Southwest Taxes Should Cover Tab Los Angeles Daily News Archived from the original on March 12 2016 Retrieved March 11 2016 City officials said Wednesday they will likely continue to push Southwest to pay the 40 000 bill for services including overtime for police officers and firefighters provided in the wake of the March 5 mishap External links editNTSB investigation docket Retrieved from https en wikipedia org w index php title Southwest Airlines Flight 1455 amp oldid 1178652091, wikipedia, wiki, book, books, library,

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