fbpx
Wikipedia

National Airlines Flight 27

National Airlines Flight 27 was a scheduled passenger flight between Miami, Florida and San Francisco, California with intermediate stops at New Orleans, Louisiana; Houston, Texas; and Las Vegas, Nevada, in the United States.

National Airlines Flight 27
N60NA, the aircraft involved in the accident.
Accident
DateNovember 3, 1973
SummaryUncontained engine failure
Siteen route over New Mexico
Aircraft
Aircraft typeMcDonnell Douglas DC-10-10
Aircraft nameBarbara[1][2]
OperatorNational Airlines (NA)
RegistrationN60NA
Flight originMiami International Airport
1st stopoverNew Orleans International Airport
2nd stopoverHouston Intercontinental Airport
3rd stopoverMcCarran International Airport
DestinationSan Francisco International Airport
Occupants128
Passengers116
Crew12
Fatalities1
Injuries24
Survivors127

On November 3, 1973, the aircraft servicing the flight, a McDonnell Douglas DC-10-10 with the tail number N60NA, experienced an uncontained engine failure, causing significant damage to the aircraft. The aircraft later managed to make a safe emergency landing at the Albuquerque International Sunport. One passenger was ejected from the aircraft at cruising altitude, in addition to minor injuries sustained by 24 passengers.

Flight crew

The crew consisted of Captain William R. Broocke (age 54), employed by National Airlines since 1946, who had qualified to fly the DC-10 in 1972 and accumulated 21,853 flight hours in his career with 801 hours on the DC-10; First Officer Edward H. Saunders (33), employed by National Airlines since 1965, with 7,086 flight hours of which 445 hours were on the DC-10; and Flight Engineer Golden W. Hanks (55), employed by National Airlines since 1950, with 17,814 flight hours of which 1,252 flight hours were on the DC-10.

Incident

On November 3, 1973, Flight 27 took off from Houston, Texas bound for Las Vegas International Airport. The aircraft leveled off at 39,000 feet (12,000 m) with an indicated airspeed of about 300 knots (350 mph; 560 km/h).

At about 16:40 MST, while the aircraft was at cruising altitude 65 miles (56 nmi; 105 km) southwest of Albuquerque, New Mexico, the No. 3 (starboard) engine fan assembly disintegrated in an uncontained catastrophic failure. Smoke was reported to fill the cabin before the fragments of the fan assembly penetrated the fuselage, the No's. 1 and 2 engine nacelles, and the right wing at high speeds, causing a cabin window to dislodge and eject the adjacent passenger from the aircraft. The resultant damage caused decompression of the aircraft cabin and the loss of certain electrical and hydraulic systems.[3]

The flight crew initiated an emergency descent, and the aircraft landed safely at Albuquerque International Sunport 19 minutes after the engine failed. 115 passengers and 12 crew members exited the aircraft by using the evacuation slides. The plane was repaired and was later flown by Pan Am (as Clipper Meteor).[citation needed]

Casualties

 
Flight 27 after the emergency landing at the Sunport

Of the 116 passengers on board, 24 people were treated by medical personnel from nearby Kirtland Air Force Base for smoke inhalation, ear problems, and minor abrasions.

One passenger[4] was partially blown into the opening made by the failed cabin window, after it too was struck by engine fragments. He was temporarily retained in that position by his seatbelt. "Efforts to pull the passenger back into the airplane by another passenger were unsuccessful, and the occupant of seat 17H was sucked entirely through the cabin window."[5]

The New Mexico State Police and local organizations searched extensively for the missing passenger who was blown out of the window. Computer analysis was made of the possible falling trajectories, which narrowed the search pattern. However, the search effort was unsuccessful. A ranch hand later found a pair of sunglasses and a tobacco pipe while working on a ranch near Alamo, New Mexico. He turned over the items to state police, where the family of the missing passenger identified them as belonging to him.

In 1975, two years after the incident, a construction crew laying the tracks for the north arm of the Very Large Array radio telescope on the Plains of San Augustin, came upon his skeletal remains. The remains took another year for the medical investigator in Albuquerque to identify.[6]

Investigation

 
Damage to the aircraft caused by the engine failure
 
N60NA's No.3 engine after the failure, showing the remains of the failed fan assembly
 
The reconstructed fan assembly that caused the engine failure

The National Transportation Safety Board determined the probable cause of this accident was the disintegration of the No. 3 engine fan assembly as a result of an interaction between the fan blade tips and the fan case. According to the NTSB, "the precise reason or reasons for the acceleration and the onset of the destructive vibration could not be determined conclusively", but enough was learned to prevent the occurrence of similar events. The speed of the engine at the time of the accident caused a resonance wave to occur in the fan assembly when the tips of the fan blades began to make contact with the surrounding shroud. The engine was designed to have a rearward blade retaining force of 18,000 pounds (8,200 kg) to prevent the blades from moving forward in their mountings slots and subsequently departing from the fan disk. The rearward force was not enough. As a result of this accident, GE re-designed the engine so that the blade retaining capability was increased to 60,000 pounds (27,000 kg), and that change was incorporated into all engines already in service.[3]

In addition to this, it was found that between August 8 and September 12, 1973, there had been 15 problems reported about the third engine.[7] The engine had been taken off the aircraft for repairs, and between the time it was replaced and the accident, a further 26 faults had been reported by the pilots. It was found that the bolts that had held the front covering in place, which had failed in the accident, were outside the tolerances laid down. An engineering dispatch was sent out to inspect these engines, and six more discrepancies were found in the National Airlines fleet alone. Therefore, this dispatch was made compulsory for all early DC-10s in order to prevent the issue from occurring again.[7]

The NTSB expressed concern about the cockpit crew conducting an unauthorized experiment on the auto-throttle system. They had been wondering where the system took its engine power readings from and to see if it was the N1 tachometer readout "the flight engineer pulled the three N1 tachometers [circuit breakers]" and then adjusted the autothrottle setting. The cockpit voice recorder proved that the engines altered their power setting when requested, proving to the crew that the system was powered from another source. The crew then manually reset the throttles to the normal cruising power before the flight engineer had closed the tachometer circuit breakers. It was considered whether the crew had accidentally over-speeded the engine when setting power without the tachometers, but there was insufficient evidence to deliver a certain verdict. Nonetheless, "regardless of the cause of the high fan speed at the time of the fan failure, the Safety Board is concerned that the flight crew was, in effect, performing an untested failure analysis on this system. This type of experimentation, without the benefit of training or specific guidelines, should never be performed during passenger flight operations."[3]

See also

References

  1. ^ Stephen Barlay. Aircrash Detective. Coronet. 1975. ISBN 0-340-19890-7
  2. ^ Macarthur Job. Air Disaster Volume 1. Aerospace Publications Pty Ltd. 1994. ISBN 1-875671-11-0
  3. ^ a b c "NTSB Report AAR75-02" (PDF). NTSB. pp. 6, 7, 8, 20, 35, 36.
  4. ^ "Featured Maps: Decompression Defenestration (3 November 2010)". Retrieved 2010-11-21.
  5. ^ Mondout, Patrick. . Archived from the original on 2011-04-08. Retrieved 2010-11-21.
  6. ^ Harden, Paul (2010-06-05). . El Defensor Chieftain. Archived from the original on 2020-08-15. Retrieved 2018-10-24.
  7. ^ a b Godson, John (1975). The rise and fall of the DC-10. D. McKay Co. p. 188. ISBN 0679505288. OCLC 1245951.

External links

  • Aviation Safety Network

national, airlines, flight, scheduled, passenger, flight, between, miami, florida, francisco, california, with, intermediate, stops, orleans, louisiana, houston, texas, vegas, nevada, united, states, n60na, aircraft, involved, accident, accidentdatenovember, 1. National Airlines Flight 27 was a scheduled passenger flight between Miami Florida and San Francisco California with intermediate stops at New Orleans Louisiana Houston Texas and Las Vegas Nevada in the United States National Airlines Flight 27N60NA the aircraft involved in the accident AccidentDateNovember 3 1973SummaryUncontained engine failureSiteen route over New MexicoAircraftAircraft typeMcDonnell Douglas DC 10 10Aircraft nameBarbara 1 2 OperatorNational Airlines NA RegistrationN60NAFlight originMiami International Airport1st stopoverNew Orleans International Airport2nd stopoverHouston Intercontinental Airport3rd stopoverMcCarran International AirportDestinationSan Francisco International AirportOccupants128Passengers116Crew12Fatalities1Injuries24Survivors127On November 3 1973 the aircraft servicing the flight a McDonnell Douglas DC 10 10 with the tail number N60NA experienced an uncontained engine failure causing significant damage to the aircraft The aircraft later managed to make a safe emergency landing at the Albuquerque International Sunport One passenger was ejected from the aircraft at cruising altitude in addition to minor injuries sustained by 24 passengers Contents 1 Flight crew 2 Incident 3 Casualties 4 Investigation 5 See also 6 References 7 External linksFlight crew EditThe crew consisted of Captain William R Broocke age 54 employed by National Airlines since 1946 who had qualified to fly the DC 10 in 1972 and accumulated 21 853 flight hours in his career with 801 hours on the DC 10 First Officer Edward H Saunders 33 employed by National Airlines since 1965 with 7 086 flight hours of which 445 hours were on the DC 10 and Flight Engineer Golden W Hanks 55 employed by National Airlines since 1950 with 17 814 flight hours of which 1 252 flight hours were on the DC 10 Incident EditOn November 3 1973 Flight 27 took off from Houston Texas bound for Las Vegas International Airport The aircraft leveled off at 39 000 feet 12 000 m with an indicated airspeed of about 300 knots 350 mph 560 km h At about 16 40 MST while the aircraft was at cruising altitude 65 miles 56 nmi 105 km southwest of Albuquerque New Mexico the No 3 starboard engine fan assembly disintegrated in an uncontained catastrophic failure Smoke was reported to fill the cabin before the fragments of the fan assembly penetrated the fuselage the No s 1 and 2 engine nacelles and the right wing at high speeds causing a cabin window to dislodge and eject the adjacent passenger from the aircraft The resultant damage caused decompression of the aircraft cabin and the loss of certain electrical and hydraulic systems 3 The flight crew initiated an emergency descent and the aircraft landed safely at Albuquerque International Sunport 19 minutes after the engine failed 115 passengers and 12 crew members exited the aircraft by using the evacuation slides The plane was repaired and was later flown by Pan Am as Clipper Meteor citation needed Casualties Edit Flight 27 after the emergency landing at the Sunport Of the 116 passengers on board 24 people were treated by medical personnel from nearby Kirtland Air Force Base for smoke inhalation ear problems and minor abrasions One passenger 4 was partially blown into the opening made by the failed cabin window after it too was struck by engine fragments He was temporarily retained in that position by his seatbelt Efforts to pull the passenger back into the airplane by another passenger were unsuccessful and the occupant of seat 17H was sucked entirely through the cabin window 5 The New Mexico State Police and local organizations searched extensively for the missing passenger who was blown out of the window Computer analysis was made of the possible falling trajectories which narrowed the search pattern However the search effort was unsuccessful A ranch hand later found a pair of sunglasses and a tobacco pipe while working on a ranch near Alamo New Mexico He turned over the items to state police where the family of the missing passenger identified them as belonging to him In 1975 two years after the incident a construction crew laying the tracks for the north arm of the Very Large Array radio telescope on the Plains of San Augustin came upon his skeletal remains The remains took another year for the medical investigator in Albuquerque to identify 6 Investigation Edit Damage to the aircraft caused by the engine failure N60NA s No 3 engine after the failure showing the remains of the failed fan assembly The reconstructed fan assembly that caused the engine failure The National Transportation Safety Board determined the probable cause of this accident was the disintegration of the No 3 engine fan assembly as a result of an interaction between the fan blade tips and the fan case According to the NTSB the precise reason or reasons for the acceleration and the onset of the destructive vibration could not be determined conclusively but enough was learned to prevent the occurrence of similar events The speed of the engine at the time of the accident caused a resonance wave to occur in the fan assembly when the tips of the fan blades began to make contact with the surrounding shroud The engine was designed to have a rearward blade retaining force of 18 000 pounds 8 200 kg to prevent the blades from moving forward in their mountings slots and subsequently departing from the fan disk The rearward force was not enough As a result of this accident GE re designed the engine so that the blade retaining capability was increased to 60 000 pounds 27 000 kg and that change was incorporated into all engines already in service 3 In addition to this it was found that between August 8 and September 12 1973 there had been 15 problems reported about the third engine 7 The engine had been taken off the aircraft for repairs and between the time it was replaced and the accident a further 26 faults had been reported by the pilots It was found that the bolts that had held the front covering in place which had failed in the accident were outside the tolerances laid down An engineering dispatch was sent out to inspect these engines and six more discrepancies were found in the National Airlines fleet alone Therefore this dispatch was made compulsory for all early DC 10s in order to prevent the issue from occurring again 7 The NTSB expressed concern about the cockpit crew conducting an unauthorized experiment on the auto throttle system They had been wondering where the system took its engine power readings from and to see if it was the N1 tachometer readout the flight engineer pulled the three N1 tachometers circuit breakers and then adjusted the autothrottle setting The cockpit voice recorder proved that the engines altered their power setting when requested proving to the crew that the system was powered from another source The crew then manually reset the throttles to the normal cruising power before the flight engineer had closed the tachometer circuit breakers It was considered whether the crew had accidentally over speeded the engine when setting power without the tachometers but there was insufficient evidence to deliver a certain verdict Nonetheless regardless of the cause of the high fan speed at the time of the fan failure the Safety Board is concerned that the flight crew was in effect performing an untested failure analysis on this system This type of experimentation without the benefit of training or specific guidelines should never be performed during passenger flight operations 3 See also EditUnited Airlines Flight 232 a 1989 accident involving a DC 10 which suffered an uncontained engine failure resulting in 112 fatalities United Airlines Flight 328 and United Airlines Flight 1175 other cases of explosive engine failures Aloha Airlines Flight 243 a 1988 incident that involved an explosive decompression of the fuselage with one fatality British Airways Flight 5390 a 1990 incident where a crew member was partially ejected from a window in flight Southwest Airlines Flight 3472 and 1380 two incidents in 2016 and 2018 respectively on two similar Boeing 737 700 both with the same engine model where the number one engine left side experienced a contained engine failure that still caused damage elsewhere in the aircraft the latter resulting in one fatality Delta Air Lines Flight 1288 another uncontained engine failure the engine exploded during takeoff killing two Air France Flight 66 a 2017 incident where an engine exploded during cruise with no injuries Qantas Flight 32 a 2010 incident where the 2 engine suffered an uncontained failure with no injuries References Edit Stephen Barlay Aircrash Detective Coronet 1975 ISBN 0 340 19890 7 Macarthur Job Air Disaster Volume 1 Aerospace Publications Pty Ltd 1994 ISBN 1 875671 11 0 a b c NTSB Report AAR75 02 PDF NTSB pp 6 7 8 20 35 36 Featured Maps Decompression Defenestration 3 November 2010 Retrieved 2010 11 21 Mondout Patrick Curious Crew Nearly Crashes DC 10 Archived from the original on 2011 04 08 Retrieved 2010 11 21 Harden Paul 2010 06 05 Aircraft Down El Defensor Chieftain Archived from the original on 2020 08 15 Retrieved 2018 10 24 a b Godson John 1975 The rise and fall of the DC 10 D McKay Co p 188 ISBN 0679505288 OCLC 1245951 External links EditPortals United States Aviation Aviation Safety Network Accident summary doc file Retrieved from https en wikipedia org w index php title National Airlines Flight 27 amp oldid 1126307730, wikipedia, wiki, book, books, library,

article

, read, download, free, free download, mp3, video, mp4, 3gp, jpg, jpeg, gif, png, picture, music, song, movie, book, game, games.