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LOT Polish Airlines Flight 007

LOT Polish Airlines Flight 007 was an Ilyushin Il-62 that crashed near Okęcie Airport in Warsaw, Poland, on 14 March 1980, as the crew aborted a landing and attempted to go-around. All 87 crew and passengers died. It was caused by the disintegration of one of the turbine discs in one of the plane's engines, leading to uncontained engine failure. The turbine disc was later found to have manufacturing faults.[1]

LOT Polish Airlines Flight 007
SP-LAA, the aircraft involved in the accident, on the apron at John F. Kennedy International Airport in 1979.
Accident
Date14 March 1980 (1980-03-14)
SummaryUncontained engine failure due to engine part with manufacturing fault, loss of flight controls
SiteNear Warsaw Okęcie Airport, Warsaw, Poland
52°11′06.5″N 20°56′46.3″E / 52.185139°N 20.946194°E / 52.185139; 20.946194
Aircraft
Aircraft typeIlyushin Il-62
Aircraft nameMikołaj Kopernik
OperatorLOT Polish Airlines
RegistrationSP-LAA
Flight originJohn F. Kennedy International Airport, New York (JFK/KJFK)
DestinationWarsaw Okęcie Airport, Warsaw, Poland (WAW/EPWA)
Occupants87
Passengers77
Crew10
Fatalities87
Injuries0
Missing0
Survivors0

The aircraft and crew edit

LOT initiated their transatlantic routes in the early 1970s, for which it decided to purchase Ilyushin Il-62s. The aircraft which crashed was the first Il-62 that LOT had purchased for this purpose, manufactured in 1971. As with all Ilyushins purchased, it was named after a famous Polish historical figure, in this case astronomer Nicolaus Copernicus (Polish: Mikołaj Kopernik).[2]

All of the crew members of Flight 007 were Polish. The captain, Paweł Lipowczan, was 46 years old, with 8,770 flight hours' experience (4,385 of them on Ilyushin Il-62s). The first officer was Tadeusz Łochocki. The remaining flight crew were flight engineer Jan Łubniewski, flight navigator Konstanty Chorzewski and radio operator Stefan Wąsiewicz. There were five flight attendants on board.

Future World Heavyweight Champion Tony Tucker was supposed to be on this flight but could not go because of a shoulder injury. All 87 people on board were killed, including 22 members of the U.S. boxing team.

Crash edit

On its final flight, the aircraft was piloted by Captain Lipowczan and First Officer Łochocki. Flight 007 was scheduled to depart from Kennedy International Airport at about 19:00 local time on 13 March 1980, but it was delayed because of a heavy snowstorm. It finally departed at 21:18, and after nine hours of an uneventful flight, it was approaching Okęcie Airport at 11:13 local time. During their final approach, about one minute before the landing, the crew reported to Okęcie Air Traffic Control that the landing gear indicator light was not operating, and that they would go around and allow the flight engineer to check if it was caused by a burnt-out fuse or light bulb, or if there was actually some problem with the gears deploying.

11:13:46 Okęcie Air Traffic Control LOT 007, 5 degrees to the right.
11:13:52 Okęcie ATC LOT 007?
11:13:54 LOT Roger that... One moment, we have some problems with landing-gear-down-and-locked indicator, request a go-around.
11:13:57 Okęcie ATC Roger, runway heading and altitude 650 metres (2,130 ft). [At that moment, "Kopernik" was at an altitude of 250 m (820 ft).]
11:14:00 LOT Runway heading and 650.

This was the last transmission from Mikołaj Kopernik. Nine seconds later, the aircraft suddenly entered a steep dive. At 11:14:35, after 26 seconds of uncontrolled descent, the aircraft clipped a tree with its right wing and impacted the ice-covered moat of a 19th-century military fortress at a speed of approximately 380 km/h (210 kn; 240 mph) at a 20-degree down angle, 950 m (3,120 ft) away from the runway threshold and 100 m (330 ft) from a residential area. At the last moment Captain Lipowczan, using nothing but the plane's ailerons, managed to avoid hitting a correctional facility for teenagers located at Rozwojowa Street. On impact, the aircraft disintegrated; a large part of the main hull submerged in the moat, while the tail and parts of the main landing gear landed a few meters further, just before the entrance to the fort. On the scene, a diving team was later trying to recover parts of the aircraft (including some of the engines) from the moat, but it was far too murky; ultimately, the moat had to be drained to allow the air crash investigation team to recover parts of the disintegrated plane. The body of Captain Lipowczan was found lying on the street about 60 m (200 ft) from the crash site; other bodies were scattered between the plane parts.

 
Graves of the crew at Powązki Military Cemetery, Warsaw.

Among the 87 fatalities were Polish singer Anna Jantar, American ethnomusicologist Alan P. Merriam, six Polish students returning home from an AIESEC conference in New York, and a contingent of the U.S. amateur boxing team (who were scheduled for a series of exhibition fights in Europe instead of the boycotted Summer Olympics.) According to the doctors who arrived at the scene, many of the passengers were apparently asleep when the plane hit the ground, but some of them – including many of the boxers – were supposedly aware that they were about to crash, as they held to their seats so strongly that on impact, the muscles and tendons in their arms became severed. Some reports suggested that some of the boxers actually survived the crash and drowned in the moat, but no evidence for this was presented. A total of 22 U.S. boxers, trainers, and doctors died in the accident (including the 1979 Pan American Games winner light welterweight Lemuel Steeples). A number of Olympic team members were not present due to various pugilistic injuries sustained before the flight or for other reasons, which prevented their participation in the scheduled event, so they stayed in the United States.

Nationality Passengers Crew Total
Poland 42 10 52
United States 28 0 28
Soviet Union 4 0 4
East Germany 3 0 3
Total 77 10 87

Investigation edit

The police quickly surrounded the site and removed any spectators; recovery of airplane pieces started soon afterwards. Both the cockpit voice recorder and flight data recorder were found quickly; unfortunately, the recording suddenly stopped nine seconds after the last transmission, 26 seconds before the crash.

While recovering the engines, the number-two (inner left) engine was found to be cut in half, held together only by the fuel lines. When the engine was further examined, the disc of the low-pressure turbine was found to be missing; despite an extensive search, it was not found at the crash site. Finally, the turbine disc was found about 4 kilometres (2.5 mi; 2.2 nmi) from the site; it was broken into three similar-sized pieces.

After recovering the cockpit, the throttles of both engines 2 and 3 (inner right) were found to be shut off, while on engine 4 (outer right) the thrust was set to maximum. The investigating commission asked the Soviets if an Il-62 was able to reach the runway with one engine operating; no conclusive answer was received, but calculations based on the official technical data suggested that, while one engine thrust was insufficient for the aircraft to maintain altitude, it was enough to reach the runway and try to land. No explanation was found why the aircraft with one engine operating at maximum power suddenly entered a steep dive.

Detailed analysis of the pieces of the turbine disc found several metallic impurities on the edges of two of them; in one case, they were identified as coming from the engine nacelle, in another, the impurities came from the nacelle, the hull, control actuators and finally, electrical cables. Also, detailed examination of the surface of the broken disc showed significant evidence of fatigue cracking.

Sequence of events edit

Finally, when the control pushers were found to be cut in half, it was proven that the cut was not caused by the crash, and some traces of the metal alloy the turbine disc was made of were found on the surface of the cut, the sequence of events became clear. The disaster started when Mikołaj Kopernik was instructed to climb to a higher flight level. When the necessary thrust was applied to all four engines, the low-pressure turbine of the number 2 engine disintegrated after 9 seconds. One piece of the turbine disc got ejected upwards, not causing any significant damage; the second piece shot into the engine number 1, damaging it seriously; finally, the third piece of the disc shot into the hull, severed the rudder and elevator control rods and destroyed the number 3 engine, causing loss of control over the plane; it also severed power cables for both the flight data recorder and the cockpit voice recorder. This caused the last moments of Mikołaj Kopernik not to be recorded.

The cut control rods also explained the sudden dive. When they were cut, the horizontal stabilizer, under its own weight, dropped down, causing the nose also to go down. This could be counteracted by the vertical trim; in Il-62s, the switch setting the vertical trim to manual operation was secured by a thin, sharp wire. On Captain Lipowczan's right hand, small wounds were found, and they were confirmed to be made while Lipowczan was still alive; supposedly, he ripped the security off and tried to control the vertical trim, but it was too late.

In an interview for Polish TV series The Black Series, Captain Tomasz Smolicz, an experienced airline pilot who flew thousands of hours on transatlantic routes on Ilyushins Il-62 and Il-62M in the 1970s and 1980s (he flew Mikołaj Kopernik from Warsaw to New York on 13 March 1980), stated that the planes returning to Warsaw from the United States usually landed on runway course 150 (150 degrees, south-south-east), and if they landed at or before noon on a sunny day (such as on 14 March 1980), the sun was shining almost directly in their eyes, which were weary after several hours of night flight and constant monitoring of cockpit instruments; this sometimes caused disorientation and confusion if an indicator light actually was lit or not; so, on that day, the landing gear indicator could have actually been lit, but the crew members might have managed to see it incorrectly. During the recovery, the landing gear was found to be properly extended and locked.

Causes of disaster edit

According to the Polish government's Special Disaster Commission, the crash was caused by defects in materials, faults in the manufacturing process of the Kuznetsov NK-8 jet engine's shaft, and weaknesses in the design of its turbine.

During the manufacturing of the low-pressure shaft, at a location where its section diameter increases, a sharp, 90-degree step was made, resulting in a sudden diameter change over a very short linear length - a classic condition for stress concentration, which results in fatigue cracking at that location. Additionally, the metallurgical analysis found that the shaft was incorrectly heat-treated during manufacture and contained contaminant particles such as non-metallic inclusions, which further reduced the shaft's ability to carry the torsional loads as designed. The improper machining and impurities facilitated an accelerated fatigue fracture of this key engine component via unmitigated formation of micro-cracks through the shaft's core, ultimately leading to its failure.

Over time, the defects in Mikołaj Kopernik's shaft became large enough, and the shaft broke, resulting in the physical separation of the low-pressure turbine from the low-pressure compressor. As a result, the low-pressure turbine explosively disintegrated. Ejected with enormous force, pieces of the turbines damaged two further engines and cut through the hull. This caused the failure of the vertical and horizontal flight controls (rudder and elevator), and a catastrophic failure of numerous systems of the aircraft. The sudden loss of control of the flight control surfaces caused a steep, unrecoverable dive, and resulted in a crash, 26 seconds from the time of the original failure.

A press article, released in Poland in 2010 and based on the review of archival documentation kept in IPN claimed that the People's Republic of Poland authorities contributed to the crash by demanding savings from LOT and excessive exploitation of engines.[3] As a result of the economic policy of Edward Gierek in People's Republic of Poland in the second half of the 1970s it began raising prices, which started to drag the country into an economic crisis. In such circumstances, the Ministry of Transport required LOT to reduce costs. One of the first measures to reduce costs was to minimize refueling planes in foreign airports due to higher jet fuel prices. Aircraft were fueled in Poland to the maximum possible take-off weight. As a result, the crew used the full length of the runway. Conversely, they had a relatively small amount of fuel in reserve on the return flight, which sometimes forced them to land in bad weather. Flights with a maximal take off weight increased engine wear, since the engines were under greater load.

Warranty service life of NK-8-4 engines was 5,000 hours (3000 to 5000 hours is typical for such engines[4]), but about half of LOT engines failed after 2000–3000 hours. Because of this, Polish pilots often called the Il-62 "flying coffins". In spite of the low reliability, the airline decided to increase overhaul life intervals to reduce the frequency of repairs, which were carried out in Soviet factories and quite expensive. LOT sent a letter to the Ilyushin Design Bureau containing the results of a test in which it was found that the engines could operate normally 8600 hours without maintenance. From the design bureau office came the answer that the Poles could fly as much as they want, but the manufacturer was responsible only for 5000 flight hours.

Increased stress on the engines and lengthening of the service interval led to growth failure. There were cases when the IL-62 flew from the United States to Warsaw without passengers, on three engines. Representatives of the technical staff at the John F. Kennedy Airport reported two similar flights in the past two years. The most common causes of failure were bending or breaking of the blades. Consequently, there were not enough serviceable engines. LOT fell into the practice of using three engines within the service interval, and a fourth beyond the interval. The investigation revealed the practice to be widespread. The airline called the fourth engines "leaders".[5]

Initially, Mikołaj Kopernik's engine 2 was installed on the aircraft SP-LAC Fryderyk Chopin, but after 1,700 hours of flying in 1975, the engine was removed due to damage of the low-pressure compressor's blade and sent for repair to the Soviet Union. After repair, the engine was placed on SP-LAB Tadeusz Kościuszko. After 5000 hours of flight, vibration was detected above the acceptable level and felt noticeably in the back of the aircraft. Therefore, in 1978 the engine was again removed for repair in Poland and subsequently installed on SP-LAA Mikołaj Kopernik. After repair, the engine accumulated 700 flight hours before the accident.

In spite of the vibrations, the defective engine was fitted to the aircraft, it being argued that the vibration level was "below acceptable standards." Before the flight to New York the aircraft was checked by mechanic Zdzisław Jarmoniak, who found that the No.1 engine had a defect in one of the turbine blades. This deformation was located in the lowest (and widest) part of the blade. The mechanic wanted to report it, but found that the defect was already marked there (noted), and the plane was subsequently allowed to fly. As he later explained to investigators, the mechanic decided that the defect was within tolerance. Engine No.3 had 8200 hours operating time without repair. The aircraft was allowed to fly to New York with three engines and only the No.4 engine was fully serviceable.

The engine shaft's disintegration edit

The Kuznetsov NK-8 is a two-spool turbofan engine with two low pressure turbines driving the fan and low pressure compressor and one high pressure turbine driving the higher stages of the compressor.

As the No. 2 engine's low-pressure shaft failed, the low-pressure turbine suddenly separated from the low-pressure compressor, freeing itself. Because the engine combustion chamber was still producing power, the suddenly freed turbine spun out of control with such enormous speed that within a fraction of a second, the centrifugal force caused the turbine to disintegrate. The enclosure of the turbine failed to contain the pieces of the turbine, which were ejected tangentially at high speed, causing severe damage to the tail section of the aircraft.

Aftermath edit

The Polish government's Special Disaster Commission sent its findings on the cause of the accident to Moscow. In response, Russian engineers and scientists stated that the reasons given were implausible and that the turbine disintegrated because of engine failure, contrary to what was stated in the Polish report. Many years later it was revealed that after Flight 7's crash, all Il-62s used by Soviet officials and VIPs had their engines discreetly replaced with newer ones. At one occasion, a Polish governmental Il-62M had had specially installed newer engines for a joint Polish-Soviet governmental trip to Beijing; after that, the engines were taken back to the Soviet Union.

The Polish commission report also called for some modernizations in the Il-62 design, most notably doubling the flight controls, so that if one system failed the plane would still be controllable. At the time, redundant controls of this kind were in general use in American and European-made airliners. This issue was never addressed by the Soviets; none of their Ilyushins of any type had installed alternate controls.

 
Memorial to the boxers who died in the plane crash

A small statue dedicated to the boxers who perished in the accident – a trigonal prism made of bronze, with a knocked-out boxer statue at the top—is located at the grounds of Warsaw sport club Skra Warszawa. An identical statue is located at the United States Olympic Training Center in Colorado Springs. The statues were funded by Thomas Kane of Printon Kane and Company and AIBA and designed by American sculptor Auldwin Thomas Schonberg.[6]

The graves of Mikołaj Kopernik's crew are located at the Powązki Military Cemetery in Warsaw. One of the streets adjacent to the crash site bears the name of Captain Paweł Lipowczan.

See also edit

References edit

  1. ^ Ranter, Harro. "ASN Aircraft accident Ilyushin Il-62 SP-LAA Warszawa-Okecie Airport (WAW)". aviation-safety.net. Aviation Safety Network. Retrieved 12 July 2020.
  2. ^ Only a portrait of Copernicus was featured on the aircraft, which was later removed.
  3. ^ [Secret truth - disaster Ił-62 Mikołaj Kopernik - Poland] (in Polish). Newsweek.pl. Archived from the original on 8 June 2011. Retrieved 1 May 2016.
  4. ^ Steel, Marlin. "Your Guide to Jet Engine Maintenance". www.marlinwire.com. Retrieved 19 April 2023.
  5. ^ "Ostatnie 26 sekund "Kopernika" - Polska" [Last 26 seconds of "Copernicus" - Poland]. n744pm.wordpress.com (in Polish). 7 March 2012.
  6. ^ "SGT ELLIOTT CHAVIS 118th Military Police Company (ABN) Ft. Bragg, North Carolina". Military Police Memorial Pages. 2004. Retrieved 19 May 2013.

All information in this entry is based on information, interviews and documents presented in two episodes of the Polish TV series "The Black Series" about air, land and marine incidents and disasters in post-war Poland: "Kopernik" (about Flight 007) and "Kościuszko" (about LOT Flight 5055).

External links edit

  • PlaneCrashInfo.Com accident report
  • Polish press article (polish language)
  • Wikipedia map disaster site
  • Materials publicized on Polish version of Wikipedia dedicated to same subject

Plane pictures edit

  • Photo of Ilyushin 62 SP-LAA
  • LOT Polish Airlines Ilyushin IL-62

Disaster site pictures edit

polish, airlines, flight, other, uses, flight, this, article, multiple, issues, please, help, improve, discuss, these, issues, talk, page, learn, when, remove, these, template, messages, this, article, needs, additional, citations, verification, please, help, . For other uses see Flight 7 This article has multiple issues Please help improve it or discuss these issues on the talk page Learn how and when to remove these template messages This article needs additional citations for verification Please help improve this article by adding citations to reliable sources Unsourced material may be challenged and removed Find sources LOT Polish Airlines Flight 007 news newspapers books scholar JSTOR March 2011 Learn how and when to remove this template message This article includes a list of general references but it lacks sufficient corresponding inline citations Please help to improve this article by introducing more precise citations July 2020 Learn how and when to remove this template message Learn how and when to remove this template message LOT Polish Airlines Flight 007 was an Ilyushin Il 62 that crashed near Okecie Airport in Warsaw Poland on 14 March 1980 as the crew aborted a landing and attempted to go around All 87 crew and passengers died It was caused by the disintegration of one of the turbine discs in one of the plane s engines leading to uncontained engine failure The turbine disc was later found to have manufacturing faults 1 LOT Polish Airlines Flight 007SP LAA the aircraft involved in the accident on the apron at John F Kennedy International Airport in 1979 AccidentDate14 March 1980 1980 03 14 SummaryUncontained engine failure due to engine part with manufacturing fault loss of flight controlsSiteNear Warsaw Okecie Airport Warsaw Poland 52 11 06 5 N 20 56 46 3 E 52 185139 N 20 946194 E 52 185139 20 946194AircraftAircraft typeIlyushin Il 62Aircraft nameMikolaj KopernikOperatorLOT Polish AirlinesRegistrationSP LAAFlight originJohn F Kennedy International Airport New York JFK KJFK DestinationWarsaw Okecie Airport Warsaw Poland WAW EPWA Occupants87Passengers77Crew10Fatalities87Injuries0Missing0Survivors0 Contents 1 The aircraft and crew 2 Crash 3 Investigation 3 1 Sequence of events 4 Causes of disaster 5 The engine shaft s disintegration 6 Aftermath 7 See also 8 References 9 External links 9 1 Plane pictures 9 2 Disaster site picturesThe aircraft and crew editThis section does not cite any sources Please help improve this section by adding citations to reliable sources Unsourced material may be challenged and removed July 2020 Learn how and when to remove this template message LOT initiated their transatlantic routes in the early 1970s for which it decided to purchase Ilyushin Il 62s The aircraft which crashed was the first Il 62 that LOT had purchased for this purpose manufactured in 1971 As with all Ilyushins purchased it was named after a famous Polish historical figure in this case astronomer Nicolaus Copernicus Polish Mikolaj Kopernik 2 All of the crew members of Flight 007 were Polish The captain Pawel Lipowczan was 46 years old with 8 770 flight hours experience 4 385 of them on Ilyushin Il 62s The first officer was Tadeusz Lochocki The remaining flight crew were flight engineer Jan Lubniewski flight navigator Konstanty Chorzewski and radio operator Stefan Wasiewicz There were five flight attendants on board Future World Heavyweight Champion Tony Tucker was supposed to be on this flight but could not go because of a shoulder injury All 87 people on board were killed including 22 members of the U S boxing team Crash editThis section does not cite any sources Please help improve this section by adding citations to reliable sources Unsourced material may be challenged and removed July 2020 Learn how and when to remove this template message On its final flight the aircraft was piloted by Captain Lipowczan and First Officer Lochocki Flight 007 was scheduled to depart from Kennedy International Airport at about 19 00 local time on 13 March 1980 but it was delayed because of a heavy snowstorm It finally departed at 21 18 and after nine hours of an uneventful flight it was approaching Okecie Airport at 11 13 local time During their final approach about one minute before the landing the crew reported to Okecie Air Traffic Control that the landing gear indicator light was not operating and that they would go around and allow the flight engineer to check if it was caused by a burnt out fuse or light bulb or if there was actually some problem with the gears deploying 11 13 46 Okecie Air Traffic Control LOT 007 5 degrees to the right 11 13 52 Okecie ATC LOT 007 11 13 54 LOT Roger that One moment we have some problems with landing gear down and locked indicator request a go around 11 13 57 Okecie ATC Roger runway heading and altitude 650 metres 2 130 ft At that moment Kopernik was at an altitude of 250 m 820 ft 11 14 00 LOT Runway heading and 650 This was the last transmission from Mikolaj Kopernik Nine seconds later the aircraft suddenly entered a steep dive At 11 14 35 after 26 seconds of uncontrolled descent the aircraft clipped a tree with its right wing and impacted the ice covered moat of a 19th century military fortress at a speed of approximately 380 km h 210 kn 240 mph at a 20 degree down angle 950 m 3 120 ft away from the runway threshold and 100 m 330 ft from a residential area At the last moment Captain Lipowczan using nothing but the plane s ailerons managed to avoid hitting a correctional facility for teenagers located at Rozwojowa Street On impact the aircraft disintegrated a large part of the main hull submerged in the moat while the tail and parts of the main landing gear landed a few meters further just before the entrance to the fort On the scene a diving team was later trying to recover parts of the aircraft including some of the engines from the moat but it was far too murky ultimately the moat had to be drained to allow the air crash investigation team to recover parts of the disintegrated plane The body of Captain Lipowczan was found lying on the street about 60 m 200 ft from the crash site other bodies were scattered between the plane parts nbsp Graves of the crew at Powazki Military Cemetery Warsaw Among the 87 fatalities were Polish singer Anna Jantar American ethnomusicologist Alan P Merriam six Polish students returning home from an AIESEC conference in New York and a contingent of the U S amateur boxing team who were scheduled for a series of exhibition fights in Europe instead of the boycotted Summer Olympics According to the doctors who arrived at the scene many of the passengers were apparently asleep when the plane hit the ground but some of them including many of the boxers were supposedly aware that they were about to crash as they held to their seats so strongly that on impact the muscles and tendons in their arms became severed Some reports suggested that some of the boxers actually survived the crash and drowned in the moat but no evidence for this was presented A total of 22 U S boxers trainers and doctors died in the accident including the 1979 Pan American Games winner light welterweight Lemuel Steeples A number of Olympic team members were not present due to various pugilistic injuries sustained before the flight or for other reasons which prevented their participation in the scheduled event so they stayed in the United States Nationality Passengers Crew TotalPoland 42 10 52United States 28 0 28Soviet Union 4 0 4East Germany 3 0 3Total 77 10 87Investigation editThis section does not cite any sources Please help improve this section by adding citations to reliable sources Unsourced material may be challenged and removed July 2020 Learn how and when to remove this template message The police quickly surrounded the site and removed any spectators recovery of airplane pieces started soon afterwards Both the cockpit voice recorder and flight data recorder were found quickly unfortunately the recording suddenly stopped nine seconds after the last transmission 26 seconds before the crash While recovering the engines the number two inner left engine was found to be cut in half held together only by the fuel lines When the engine was further examined the disc of the low pressure turbine was found to be missing despite an extensive search it was not found at the crash site Finally the turbine disc was found about 4 kilometres 2 5 mi 2 2 nmi from the site it was broken into three similar sized pieces After recovering the cockpit the throttles of both engines 2 and 3 inner right were found to be shut off while on engine 4 outer right the thrust was set to maximum The investigating commission asked the Soviets if an Il 62 was able to reach the runway with one engine operating no conclusive answer was received but calculations based on the official technical data suggested that while one engine thrust was insufficient for the aircraft to maintain altitude it was enough to reach the runway and try to land No explanation was found why the aircraft with one engine operating at maximum power suddenly entered a steep dive Detailed analysis of the pieces of the turbine disc found several metallic impurities on the edges of two of them in one case they were identified as coming from the engine nacelle in another the impurities came from the nacelle the hull control actuators and finally electrical cables Also detailed examination of the surface of the broken disc showed significant evidence of fatigue cracking Sequence of events edit Finally when the control pushers were found to be cut in half it was proven that the cut was not caused by the crash and some traces of the metal alloy the turbine disc was made of were found on the surface of the cut the sequence of events became clear The disaster started when Mikolaj Kopernik was instructed to climb to a higher flight level When the necessary thrust was applied to all four engines the low pressure turbine of the number 2 engine disintegrated after 9 seconds One piece of the turbine disc got ejected upwards not causing any significant damage the second piece shot into the engine number 1 damaging it seriously finally the third piece of the disc shot into the hull severed the rudder and elevator control rods and destroyed the number 3 engine causing loss of control over the plane it also severed power cables for both the flight data recorder and the cockpit voice recorder This caused the last moments of Mikolaj Kopernik not to be recorded The cut control rods also explained the sudden dive When they were cut the horizontal stabilizer under its own weight dropped down causing the nose also to go down This could be counteracted by the vertical trim in Il 62s the switch setting the vertical trim to manual operation was secured by a thin sharp wire On Captain Lipowczan s right hand small wounds were found and they were confirmed to be made while Lipowczan was still alive supposedly he ripped the security off and tried to control the vertical trim but it was too late In an interview for Polish TV series The Black Series Captain Tomasz Smolicz an experienced airline pilot who flew thousands of hours on transatlantic routes on Ilyushins Il 62 and Il 62M in the 1970s and 1980s he flew Mikolaj Kopernik from Warsaw to New York on 13 March 1980 stated that the planes returning to Warsaw from the United States usually landed on runway course 150 150 degrees south south east and if they landed at or before noon on a sunny day such as on 14 March 1980 the sun was shining almost directly in their eyes which were weary after several hours of night flight and constant monitoring of cockpit instruments this sometimes caused disorientation and confusion if an indicator light actually was lit or not so on that day the landing gear indicator could have actually been lit but the crew members might have managed to see it incorrectly During the recovery the landing gear was found to be properly extended and locked Causes of disaster editThis section needs additional citations for verification Please help improve this article by adding citations to reliable sources in this section Unsourced material may be challenged and removed July 2020 Learn how and when to remove this template message This section may be confusing or unclear to readers Please help clarify the section There might be a discussion about this on the talk page May 2018 Learn how and when to remove this template message According to the Polish government s Special Disaster Commission the crash was caused by defects in materials faults in the manufacturing process of the Kuznetsov NK 8 jet engine s shaft and weaknesses in the design of its turbine During the manufacturing of the low pressure shaft at a location where its section diameter increases a sharp 90 degree step was made resulting in a sudden diameter change over a very short linear length a classic condition for stress concentration which results in fatigue cracking at that location Additionally the metallurgical analysis found that the shaft was incorrectly heat treated during manufacture and contained contaminant particles such as non metallic inclusions which further reduced the shaft s ability to carry the torsional loads as designed The improper machining and impurities facilitated an accelerated fatigue fracture of this key engine component via unmitigated formation of micro cracks through the shaft s core ultimately leading to its failure Over time the defects in Mikolaj Kopernik s shaft became large enough and the shaft broke resulting in the physical separation of the low pressure turbine from the low pressure compressor As a result the low pressure turbine explosively disintegrated Ejected with enormous force pieces of the turbines damaged two further engines and cut through the hull This caused the failure of the vertical and horizontal flight controls rudder and elevator and a catastrophic failure of numerous systems of the aircraft The sudden loss of control of the flight control surfaces caused a steep unrecoverable dive and resulted in a crash 26 seconds from the time of the original failure A press article released in Poland in 2010 and based on the review of archival documentation kept in IPN claimed that the People s Republic of Poland authorities contributed to the crash by demanding savings from LOT and excessive exploitation of engines 3 As a result of the economic policy of Edward Gierek in People s Republic of Poland in the second half of the 1970s it began raising prices which started to drag the country into an economic crisis In such circumstances the Ministry of Transport required LOT to reduce costs One of the first measures to reduce costs was to minimize refueling planes in foreign airports due to higher jet fuel prices Aircraft were fueled in Poland to the maximum possible take off weight As a result the crew used the full length of the runway Conversely they had a relatively small amount of fuel in reserve on the return flight which sometimes forced them to land in bad weather Flights with a maximal take off weight increased engine wear since the engines were under greater load Warranty service life of NK 8 4 engines was 5 000 hours 3000 to 5000 hours is typical for such engines 4 but about half of LOT engines failed after 2000 3000 hours Because of this Polish pilots often called the Il 62 flying coffins In spite of the low reliability the airline decided to increase overhaul life intervals to reduce the frequency of repairs which were carried out in Soviet factories and quite expensive LOT sent a letter to the Ilyushin Design Bureau containing the results of a test in which it was found that the engines could operate normally 8600 hours without maintenance From the design bureau office came the answer that the Poles could fly as much as they want but the manufacturer was responsible only for 5000 flight hours Increased stress on the engines and lengthening of the service interval led to growth failure There were cases when the IL 62 flew from the United States to Warsaw without passengers on three engines Representatives of the technical staff at the John F Kennedy Airport reported two similar flights in the past two years The most common causes of failure were bending or breaking of the blades Consequently there were not enough serviceable engines LOT fell into the practice of using three engines within the service interval and a fourth beyond the interval The investigation revealed the practice to be widespread The airline called the fourth engines leaders 5 Initially Mikolaj Kopernik s engine 2 was installed on the aircraft SP LAC Fryderyk Chopin but after 1 700 hours of flying in 1975 the engine was removed due to damage of the low pressure compressor s blade and sent for repair to the Soviet Union After repair the engine was placed on SP LAB Tadeusz Kosciuszko After 5000 hours of flight vibration was detected above the acceptable level and felt noticeably in the back of the aircraft Therefore in 1978 the engine was again removed for repair in Poland and subsequently installed on SP LAA Mikolaj Kopernik After repair the engine accumulated 700 flight hours before the accident In spite of the vibrations the defective engine was fitted to the aircraft it being argued that the vibration level was below acceptable standards Before the flight to New York the aircraft was checked by mechanic Zdzislaw Jarmoniak who found that the No 1 engine had a defect in one of the turbine blades This deformation was located in the lowest and widest part of the blade The mechanic wanted to report it but found that the defect was already marked there noted and the plane was subsequently allowed to fly As he later explained to investigators the mechanic decided that the defect was within tolerance Engine No 3 had 8200 hours operating time without repair The aircraft was allowed to fly to New York with three engines and only the No 4 engine was fully serviceable The engine shaft s disintegration editThis section does not cite any sources Please help improve this section by adding citations to reliable sources Unsourced material may be challenged and removed July 2020 Learn how and when to remove this template message The Kuznetsov NK 8 is a two spool turbofan engine with two low pressure turbines driving the fan and low pressure compressor and one high pressure turbine driving the higher stages of the compressor As the No 2 engine s low pressure shaft failed the low pressure turbine suddenly separated from the low pressure compressor freeing itself Because the engine combustion chamber was still producing power the suddenly freed turbine spun out of control with such enormous speed that within a fraction of a second the centrifugal force caused the turbine to disintegrate The enclosure of the turbine failed to contain the pieces of the turbine which were ejected tangentially at high speed causing severe damage to the tail section of the aircraft Aftermath editThe Polish government s Special Disaster Commission sent its findings on the cause of the accident to Moscow In response Russian engineers and scientists stated that the reasons given were implausible and that the turbine disintegrated because of engine failure contrary to what was stated in the Polish report Many years later it was revealed that after Flight 7 s crash all Il 62s used by Soviet officials and VIPs had their engines discreetly replaced with newer ones At one occasion a Polish governmental Il 62M had had specially installed newer engines for a joint Polish Soviet governmental trip to Beijing after that the engines were taken back to the Soviet Union The Polish commission report also called for some modernizations in the Il 62 design most notably doubling the flight controls so that if one system failed the plane would still be controllable At the time redundant controls of this kind were in general use in American and European made airliners This issue was never addressed by the Soviets none of their Ilyushins of any type had installed alternate controls nbsp Memorial to the boxers who died in the plane crashA small statue dedicated to the boxers who perished in the accident a trigonal prism made of bronze with a knocked out boxer statue at the top is located at the grounds of Warsaw sport club Skra Warszawa An identical statue is located at the United States Olympic Training Center in Colorado Springs The statues were funded by Thomas Kane of Printon Kane and Company and AIBA and designed by American sculptor Auldwin Thomas Schonberg 6 The graves of Mikolaj Kopernik s crew are located at the Powazki Military Cemetery in Warsaw One of the streets adjacent to the crash site bears the name of Captain Pawel Lipowczan See also edit nbsp Poland portal nbsp Aviation portal nbsp 1980s portalList of accidents and incidents involving commercial aircraft Air Algerie Flight 6289 Dana Air Flight 992 List of accidents involving sports teams LOT Polish Airlines Flight 5055 caused by failure of an engine s bearings Baikal Airlines Flight 130 United Airlines Flight 232 caused by an engine explosion due to a fatigue crack in a fan assembly Eastern Air Lines Flight 401References edit Ranter Harro ASN Aircraft accident Ilyushin Il 62 SP LAA Warszawa Okecie Airport WAW aviation safety net Aviation Safety Network Retrieved 12 July 2020 Only a portrait of Copernicus was featured on the aircraft which was later removed Zatajona prawda katastrofa Il 62 Mikolaj Kopernik Polska Secret truth disaster Il 62 Mikolaj Kopernik Poland in Polish Newsweek pl Archived from the original on 8 June 2011 Retrieved 1 May 2016 Steel Marlin Your Guide to Jet Engine Maintenance www marlinwire com Retrieved 19 April 2023 Ostatnie 26 sekund Kopernika Polska Last 26 seconds of Copernicus Poland n744pm wordpress com in Polish 7 March 2012 SGT ELLIOTT CHAVIS 118th Military Police Company ABN Ft Bragg North Carolina Military Police Memorial Pages 2004 Retrieved 19 May 2013 All information in this entry is based on information interviews and documents presented in two episodes of the Polish TV series The Black Series about air land and marine incidents and disasters in post war Poland Kopernik about Flight 007 and Kosciuszko about LOT Flight 5055 External links editAccident description at the Aviation Safety Network nbsp Wikimedia Commons has media related to 1980 LOT 007 crash PlaneCrashInfo Com accident report Polish press article polish language Wikipedia map disaster site Materials publicized on Polish version of Wikipedia dedicated to same subjectPlane pictures edit Photo of Ilyushin 62 SP LAA LOT Polish Airlines Ilyushin IL 62Disaster site pictures edit PlaneCrashInfo Com photo and report http republika pl blog ft 239514 338340 tr kopernik jpg http republika pl blog ft 239514 338340 tr kopernik1 jpg Retrieved from https en wikipedia org w index php title LOT Polish Airlines Flight 007 amp oldid 1188376932, wikipedia, wiki, book, books, library,

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