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FedEx Express Flight 14

FedEx Express Flight 14 was a scheduled cargo flight from Singapore to Newark, New Jersey, via Malaysia, Taiwan, and Alaska. On July 31, 1997, the aircraft flying this route crashed during landing on its final segment at Newark International Airport (EWR), inverting and catching fire, injuring all five people on board.[1]

FedEx Express Flight 14
The wreckage of Flight 14 after the fire was extinguished
Accident
DateJuly 31, 1997 (1997-07-31)
SummaryCrashed following hard landing
SiteNewark International Airport runway 22R, Newark, New Jersey, United States
40°41′14″N 74°10′27″W / 40.6872°N 74.1742°W / 40.6872; -74.1742
Aircraft
Aircraft typeMcDonnell Douglas MD-11F
Aircraft nameJoshua
OperatorFedEx Express
IATA flight No.FX14
ICAO flight No.FDX14
Call signFEDEX 14
RegistrationN611FE
Flight originSingapore Changi Airport, Singapore
1st stopoverPenang International Airport, Penang, Malaysia
2nd stopoverTaiwan Taoyuan International Airport, Taipei, Taiwan
Last stopoverAnchorage International Airport, Anchorage Alaska, United States
DestinationNewark International Airport,
Newark, New Jersey, United States
Occupants5
Passengers3
Crew2
Fatalities0
Injuries5
Survivors5

Summary edit

Flight 14 crashed while landing on runway 22R at Newark Airport on July 31, 1997. The flight originated in Singapore with intermediate stops in Penang, Malaysia, followed by Taipei, Taiwan, and then Anchorage, Alaska. In addition to the Captain and First Officer there were three passengers on board, including one riding in the jump seat.

During the flight, the pilots were concerned that they would have little stopping distance after landing, and the captain said that he wanted to put the aircraft down early on the runway. The aircraft had departed with one thrust reverser (on the left engine) inoperative, and the pilots knew of incidents in the aircraft's maintenance log where the auto-brakes had failed to activate during landings. They had also misinterpreted the runway data, and so believed they had less stopping distance than was actually available.[2][3]

The landing was normal until the beginning of the flare phase. The MD-11 touched down, bounced, and rolled to the right. On the second touchdown, about 1,100 feet (340 m) later, the right gear snapped and the No. 3 engine (right wing engine) contacted the runway, with the right roll continuing until the right wing spars broke. The aircraft came to rest off the right side of the runway, on its back, and on fire. All five occupants escaped through a cockpit window. The airplane was destroyed by fire.[3][4]

Aircraft and crew edit

 
N611FE, the aircraft involved in the accident, 11 months before the crash from previous livery

The aircraft, named Joshua by FedEx, construction number 48603 and line number 553, was a McDonnell Douglas MD-11F freight model, powered by three General Electric CF6-80C2D1F engines. Registered in the United States as N611FE,[5] the aircraft was delivered new to FedEx in September 1993. Prior to the crash, the aircraft had a total of 13,034 flight hours and 2,950 flight cycles (a flight cycle is defined as a takeoff and landing), and had been involved in two prior incidents. In January 1994, when it sustained underbelly damage during a bounced landing at Memphis International Airport. Then in November 1994, the aircraft was involved in a tailstrike at Anchorage International Airport. Permanent repairs were made from the Anchorage incident within days of the tailstrike, and permanent repairs to the Memphis incident were made at the next C check in August 1995.[2]

The captain was 46-year-old Robert M. Freeman who joined FedEx in 1988 when it bought Flying Tiger Line, which he had previously worked for since 1978. Freeman had logged a total of 11,000 flight hours, including 1,253 hours on the MD-11. The first officer was 39-year-old Donald E. Goodin, who had been with FedEx since 1994, having served as a former U.S. Air Force pilot from 1977 to 1994 and had 3,703 flight hours, though only 592 of them were with FedEx. Goodin only had 95 hours on the MD-11.[2]: 11–12 [6][7][8]

Investigation edit

The National Transportation Safety Board (NTSB) conducted a full investigation of the accident and concluded that the probable cause was the captain's over-control of the aircraft during the landing and his failure to go around after a destabilized flare. Beginning about 17 feet (5.2 m) above the runway, the captain had let the nose lower, probably to achieve an earlier touchdown, then raised it and increased thrust to slow the plane's descent, then pushed the nose down again (around the time of the first touchdown) to try to keep the plane on the runway. These last control inputs were "too late and too large" to stabilize the landing, and the plane's high sink rate and rightward roll compressed the right landing gear strut at the second touchdown, which broke the right wing rear spar and ruptured the right fuel tank.[2][3][4]

Safety recommendations edit

As a result of its investigation of this accident, the NTSB made new recommendations based on their findings and conclusions to improve the safety of operations of the MD-11 type aircraft including that the FAA develop new pilot training tools to "include information about factors that can contribute to structural failures involving the landing gear, wings, and fuselage, such as design sink rate limits; roll angle limits; control inputs' roll rate; pitch rate; single-gear landings; the effect of decreased lift; and structural loading consequences of bottoming landing gear struts and tires; provide a syllabus for simulator training on the execution of stabilized approaches to the landing flare, the identification of unstabilized landing flares, and recovery from these situations, including proper high sink rate recovery techniques during flare to landing, techniques for avoiding and recovering from overcontrol in pitch before touchdown, and techniques for avoiding overcontrol and premature derotation during a bounced landing; and to promote an orientation toward a proactive go-around."[2][3][4]

Aftermath edit

For his role in the accident, Captain Freeman was fired from FedEx on October 30, 2000. However, the FedEx pilot union criticized the decision and announced that they would appeal it, citing that the crash was caused by aircraft design flaws.[9]

Media edit

The crashes of FedEx Express Flight 14, and a similar crash in 2009 of another McDonnell Douglas MD-11, FedEx Express Flight 80 at Narita International Airport in Japan, are both covered on Season 14 of Mayday (Air Crash Investigation, Air Disasters), episode 5, titled "The Final Push".

See also edit

References edit

  1. ^ Ranter, Harro. "ASN Aircraft accident McDonnell Douglas MD-11F N611FE Newark International Airport, NJ (EWR)". aviation-safety.net. Aviation Safety Network. Retrieved May 19, 2020.
  2. ^ a b c d e Crash During Landing, Federal Express, Inc. McDonnell Douglas MD-11, N611FE, Newark International Airport, Newark, New Jersey, July 31, 1997 (PDF). National Transportation Safety Board. July 25, 2000. NTSB/AAR-00/02. Retrieved December 27, 2017.
  3. ^ a b c d "Destabilized Approach Results in MD-11 Bounced Landing, Structural Failure" (PDF). Accident Prevention. 58 (1). Alexandria, VA: Flight Safety Foundation. January 2001.
  4. ^ a b c Dismukes, Key; Berman, Benjamin A.; Loukopoulos, Loukia D. (January 1, 2007). The Limits of Expertise: Rethinking Pilot Error and the Causes of Airline Accidents. Hampshire, UK: Ashgate Publishing, Ltd. pp. 85–94. ISBN 978-0-7546-4965-6 – via Google Books.{{cite book}}: CS1 maint: date and year (link)
  5. ^ "FAA Registry (N611FE)". Federal Aviation Administration.
  6. ^ "Operations 2 - Group Chairman Factual Report" (PDF). National Transportation Safety Board. November 21, 1997. Retrieved May 19, 2020.
  7. ^ . www.joc.com. Associated Press. July 25, 2000. Archived from the original on December 4, 2022. Retrieved May 19, 2020.
  8. ^ "PILOT SAW HARD LANDING BEFORE NEWARK CRASH A 1997 FEDEX FLIGHT WENT FROM ROUTINE TO LIFE-THREATENING IN A MATTER OF MINUTES". Greensboro News and Record. Washington. Associated Press. December 2, 1998. Retrieved May 19, 2020.
  9. ^ . boards.fool.com. Knight Ridder/Tribune Business News. November 9, 2000. Archived from the original on January 9, 2021. Retrieved May 19, 2020.

  This article incorporates public domain material from websites or documents of the National Transportation Safety Board.

External links edit

fedex, express, flight, scheduled, cargo, flight, from, singapore, newark, jersey, malaysia, taiwan, alaska, july, 1997, aircraft, flying, this, route, crashed, during, landing, final, segment, newark, international, airport, inverting, catching, fire, injurin. FedEx Express Flight 14 was a scheduled cargo flight from Singapore to Newark New Jersey via Malaysia Taiwan and Alaska On July 31 1997 the aircraft flying this route crashed during landing on its final segment at Newark International Airport EWR inverting and catching fire injuring all five people on board 1 FedEx Express Flight 14The wreckage of Flight 14 after the fire was extinguishedAccidentDateJuly 31 1997 1997 07 31 SummaryCrashed following hard landingSiteNewark International Airport runway 22R Newark New Jersey United States 40 41 14 N 74 10 27 W 40 6872 N 74 1742 W 40 6872 74 1742AircraftAircraft typeMcDonnell Douglas MD 11FAircraft nameJoshuaOperatorFedEx ExpressIATA flight No FX14ICAO flight No FDX14Call signFEDEX 14RegistrationN611FEFlight originSingapore Changi Airport Singapore1st stopoverPenang International Airport Penang Malaysia2nd stopoverTaiwan Taoyuan International Airport Taipei TaiwanLast stopoverAnchorage International Airport Anchorage Alaska United StatesDestinationNewark International Airport Newark New Jersey United StatesOccupants5Passengers3Crew2Fatalities0Injuries5Survivors5 Contents 1 Summary 2 Aircraft and crew 3 Investigation 3 1 Safety recommendations 4 Aftermath 5 Media 6 See also 7 References 8 External linksSummary editFlight 14 crashed while landing on runway 22R at Newark Airport on July 31 1997 The flight originated in Singapore with intermediate stops in Penang Malaysia followed by Taipei Taiwan and then Anchorage Alaska In addition to the Captain and First Officer there were three passengers on board including one riding in the jump seat During the flight the pilots were concerned that they would have little stopping distance after landing and the captain said that he wanted to put the aircraft down early on the runway The aircraft had departed with one thrust reverser on the left engine inoperative and the pilots knew of incidents in the aircraft s maintenance log where the auto brakes had failed to activate during landings They had also misinterpreted the runway data and so believed they had less stopping distance than was actually available 2 3 The landing was normal until the beginning of the flare phase The MD 11 touched down bounced and rolled to the right On the second touchdown about 1 100 feet 340 m later the right gear snapped and the No 3 engine right wing engine contacted the runway with the right roll continuing until the right wing spars broke The aircraft came to rest off the right side of the runway on its back and on fire All five occupants escaped through a cockpit window The airplane was destroyed by fire 3 4 Aircraft and crew edit nbsp N611FE the aircraft involved in the accident 11 months before the crash from previous livery The aircraft named Joshua by FedEx construction number 48603 and line number 553 was a McDonnell Douglas MD 11F freight model powered by three General Electric CF6 80C2D1F engines Registered in the United States as N611FE 5 the aircraft was delivered new to FedEx in September 1993 Prior to the crash the aircraft had a total of 13 034 flight hours and 2 950 flight cycles a flight cycle is defined as a takeoff and landing and had been involved in two prior incidents In January 1994 when it sustained underbelly damage during a bounced landing at Memphis International Airport Then in November 1994 the aircraft was involved in a tailstrike at Anchorage International Airport Permanent repairs were made from the Anchorage incident within days of the tailstrike and permanent repairs to the Memphis incident were made at the next C check in August 1995 2 The captain was 46 year old Robert M Freeman who joined FedEx in 1988 when it bought Flying Tiger Line which he had previously worked for since 1978 Freeman had logged a total of 11 000 flight hours including 1 253 hours on the MD 11 The first officer was 39 year old Donald E Goodin who had been with FedEx since 1994 having served as a former U S Air Force pilot from 1977 to 1994 and had 3 703 flight hours though only 592 of them were with FedEx Goodin only had 95 hours on the MD 11 2 11 12 6 7 8 Investigation editThe National Transportation Safety Board NTSB conducted a full investigation of the accident and concluded that the probable cause was the captain s over control of the aircraft during the landing and his failure to go around after a destabilized flare Beginning about 17 feet 5 2 m above the runway the captain had let the nose lower probably to achieve an earlier touchdown then raised it and increased thrust to slow the plane s descent then pushed the nose down again around the time of the first touchdown to try to keep the plane on the runway These last control inputs were too late and too large to stabilize the landing and the plane s high sink rate and rightward roll compressed the right landing gear strut at the second touchdown which broke the right wing rear spar and ruptured the right fuel tank 2 3 4 Safety recommendations edit As a result of its investigation of this accident the NTSB made new recommendations based on their findings and conclusions to improve the safety of operations of the MD 11 type aircraft including that the FAA develop new pilot training tools to include information about factors that can contribute to structural failures involving the landing gear wings and fuselage such as design sink rate limits roll angle limits control inputs roll rate pitch rate single gear landings the effect of decreased lift and structural loading consequences of bottoming landing gear struts and tires provide a syllabus for simulator training on the execution of stabilized approaches to the landing flare the identification of unstabilized landing flares and recovery from these situations including proper high sink rate recovery techniques during flare to landing techniques for avoiding and recovering from overcontrol in pitch before touchdown and techniques for avoiding overcontrol and premature derotation during a bounced landing and to promote an orientation toward a proactive go around 2 3 4 Aftermath editFor his role in the accident Captain Freeman was fired from FedEx on October 30 2000 However the FedEx pilot union criticized the decision and announced that they would appeal it citing that the crash was caused by aircraft design flaws 9 Media editThe crashes of FedEx Express Flight 14 and a similar crash in 2009 of another McDonnell Douglas MD 11 FedEx Express Flight 80 at Narita International Airport in Japan are both covered on Season 14 of Mayday Air Crash Investigation Air Disasters episode 5 titled The Final Push See also editFedEx Express Flight 80 an MD 11 that bounced and flipped on landing in 2009 Fine Air Flight 101 a DC 8 freighter that crashed a week later in Miami List of accidents and incidents involving commercial aircraftReferences edit Ranter Harro ASN Aircraft accident McDonnell Douglas MD 11F N611FE Newark International Airport NJ EWR aviation safety net Aviation Safety Network Retrieved May 19 2020 a b c d e Crash During Landing Federal Express Inc McDonnell Douglas MD 11 N611FE Newark International Airport Newark New Jersey July 31 1997 PDF National Transportation Safety Board July 25 2000 NTSB AAR 00 02 Retrieved December 27 2017 a b c d Destabilized Approach Results in MD 11 Bounced Landing Structural Failure PDF Accident Prevention 58 1 Alexandria VA Flight Safety Foundation January 2001 a b c Dismukes Key Berman Benjamin A Loukopoulos Loukia D January 1 2007 The Limits of Expertise Rethinking Pilot Error and the Causes of Airline Accidents Hampshire UK Ashgate Publishing Ltd pp 85 94 ISBN 978 0 7546 4965 6 via Google Books a href Template Cite book html title Template Cite book cite book a CS1 maint date and year link FAA Registry N611FE Federal Aviation Administration Operations 2 Group Chairman Factual Report PDF National Transportation Safety Board November 21 1997 Retrieved May 19 2020 NTSB DISCUSSES 1997 FEDEX CRASH AT NEWARK www joc com Associated Press July 25 2000 Archived from the original on December 4 2022 Retrieved May 19 2020 PILOT SAW HARD LANDING BEFORE NEWARK CRASH A 1997 FEDEX FLIGHT WENT FROM ROUTINE TO LIFE THREATENING IN A MATTER OF MINUTES Greensboro News and Record Washington Associated Press December 2 1998 Retrieved May 19 2020 TMF Union Contests Firing of FedEx MD 11 Pilot Fedex Corp boards fool com Knight Ridder Tribune Business News November 9 2000 Archived from the original on January 9 2021 Retrieved May 19 2020 nbsp This article incorporates public domain material from websites or documents of the National Transportation Safety Board External links editNTSB investigation docket Accident description at the Aviation Safety Network Retrieved from https en wikipedia org w index php title FedEx Express Flight 14 amp oldid 1223417931, wikipedia, wiki, book, books, library,

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