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Cowan rail accident

The Cowan rail accident occurred at 7:20pm on 6 May 1990 when the 3801 Limited special steam passenger train returning from the Morpeth Jazz Festival was struck in the rear by the following CityRail inter-urban passenger service. The steam train had stalled while attempting to climb the steep gradient from the Hawkesbury River to Cowan, New South Wales, and it was found that sand applied to the rails to regain traction had interfered with the signals and given the following train a false clear indication.

Cowan rail accident
Details
Date6 May 1990
7:20 pm
LocationBrooklyn, New South Wales
Coordinates33°33′16″S 151°11′47″E / 33.55432°S 151.19633°E / -33.55432; 151.19633
CountryAustralia
LineNewcastle and Central Coast railway line
Operator3801 Limited, CityRail
Incident typeCollision
CauseSignaling fault
Statistics
Trains2
Deaths6
Injured106

Overview

The crash occurred approximately 5 kilometres (3.1 mi) south of Brooklyn, New South Wales, near the Boronia No. 3 tunnel. The railway line at this point, known as the Cowan Bank, is 2.5% (1 in 40) grade and, as the special hauled by steam locomotive 3801 passed southwards through the No. 3 tunnel, the wheels of the locomotive started to slip. The driver of 3801 applied sand to the rails to improve traction, but the train came to a complete stop approximately 50 metres clear of the tunnel. Passengers on the steam train reported seeing a signal fluctuating aspects between green and yellow. The following CityRail V set inter-urban train, which had been halted at the northern entrance to Boronia No. 4 tunnel for 10 minutes by a red stop signal, received a green indication and proceeded, colliding with the steam train shortly after.

The impact killed the driver of the inter-urban train, Gordon Hill, and a passenger who was riding in its cab, as well as four passengers in the rear carriage of 3801's train. The passengers killed were the recently retired Vice Chancellor of the University of Sydney, John Manning Ward, his wife and daughter, and the wife of the University's Registrar.[1] 99 passengers were injured, 11 of those seriously. The force of the crash completely destroyed the last carriage of the steam train, and was enough to break the locomotive coupling and push the engine 12 metres forward.

A subsequent coronial inquiry, headed by NSW State Coroner Derrick Hand, found in December 1990 that the sand that had been applied to the track by 3801 to aid traction had insulated the train from the rails, meaning that the track circuits failed to detect the presence of the first train, allowing the following inter-urban train to be given a false green (clear) aspect (known as a wrong-side failure). Mr Hand also considered it likely that a passenger on 3801 had applied a handbrake on the third carriage, and that this, combined with the heavy load, the steep grade and the curvature of the line, had prevented the steam train from restarting. No fault was found with the signalling system, although the coroner recommended that it be upgraded as soon as possible.

Contributing factors

Contributing factors include:

  • AC track circuits, which are less sensitive[citation needed] at detecting rail vehicles.
  • Sand on the rails insulated the train's wheels and prevented the track circuit from detecting it - the train effectively became invisible to the signalling system.
  • The signalling system was two-aspect colour light - a three aspect colour light may have provided the driver of the following train with more warning.
  • No sand removal system fitted to 3801.
  • No mechanism (at the time) for train-to-train or train-to-signalman communication (communication with signal boxes was only possible by track-side phones).
  • It is believed that the handbrakes on one of the carriages may have been applied as a stunt.[2]

Consequences

  • An interim ban was placed on the use of steam locomotives on the NSW railway system. The ban was lifted 9 months later.
  • Operators were required to use one State Rail employee on each train
  • Operators were required to carry insurance cover of $10 million. The government agreed to underwrite any claims exceeding that amount.

See also

References

  1. ^ Fellows of Senate: John Manning Ward AO, Memorial Service, http://sydney.edu.au/senate/Ward_memorial.shtml, Retrieved 17 February 2013
  2. ^ Pearce, Kenn (1999). Australian railway disasters (2nd ed.). IPL Books. ISBN 978-0-908876-09-9.
  • . Emergency Management NSW. Archived from the original on 2 October 2013. Retrieved 15 September 2010.
  • "RAIL SAFETY ACT 1993 NEW SOUTH WALES". Retrieved 15 September 2010.

cowan, rail, accident, occurred, 20pm, 1990, when, 3801, limited, special, steam, passenger, train, returning, from, morpeth, jazz, festival, struck, rear, following, cityrail, inter, urban, passenger, service, steam, train, stalled, while, attempting, climb, . The Cowan rail accident occurred at 7 20pm on 6 May 1990 when the 3801 Limited special steam passenger train returning from the Morpeth Jazz Festival was struck in the rear by the following CityRail inter urban passenger service The steam train had stalled while attempting to climb the steep gradient from the Hawkesbury River to Cowan New South Wales and it was found that sand applied to the rails to regain traction had interfered with the signals and given the following train a false clear indication Cowan rail accidentDetailsDate6 May 1990 7 20 pmLocationBrooklyn New South WalesCoordinates33 33 16 S 151 11 47 E 33 55432 S 151 19633 E 33 55432 151 19633CountryAustraliaLineNewcastle and Central Coast railway lineOperator3801 Limited CityRailIncident typeCollisionCauseSignaling faultStatisticsTrains2Deaths6Injured106 Contents 1 Overview 2 Contributing factors 3 Consequences 4 See also 5 ReferencesOverview EditThe crash occurred approximately 5 kilometres 3 1 mi south of Brooklyn New South Wales near the Boronia No 3 tunnel The railway line at this point known as the Cowan Bank is 2 5 1 in 40 grade and as the special hauled by steam locomotive 3801 passed southwards through the No 3 tunnel the wheels of the locomotive started to slip The driver of 3801 applied sand to the rails to improve traction but the train came to a complete stop approximately 50 metres clear of the tunnel Passengers on the steam train reported seeing a signal fluctuating aspects between green and yellow The following CityRail V set inter urban train which had been halted at the northern entrance to Boronia No 4 tunnel for 10 minutes by a red stop signal received a green indication and proceeded colliding with the steam train shortly after The impact killed the driver of the inter urban train Gordon Hill and a passenger who was riding in its cab as well as four passengers in the rear carriage of 3801 s train The passengers killed were the recently retired Vice Chancellor of the University of Sydney John Manning Ward his wife and daughter and the wife of the University s Registrar 1 99 passengers were injured 11 of those seriously The force of the crash completely destroyed the last carriage of the steam train and was enough to break the locomotive coupling and push the engine 12 metres forward A subsequent coronial inquiry headed by NSW State Coroner Derrick Hand found in December 1990 that the sand that had been applied to the track by 3801 to aid traction had insulated the train from the rails meaning that the track circuits failed to detect the presence of the first train allowing the following inter urban train to be given a false green clear aspect known as a wrong side failure Mr Hand also considered it likely that a passenger on 3801 had applied a handbrake on the third carriage and that this combined with the heavy load the steep grade and the curvature of the line had prevented the steam train from restarting No fault was found with the signalling system although the coroner recommended that it be upgraded as soon as possible Contributing factors EditContributing factors include AC track circuits which are less sensitive citation needed at detecting rail vehicles Sand on the rails insulated the train s wheels and prevented the track circuit from detecting it the train effectively became invisible to the signalling system The signalling system was two aspect colour light a three aspect colour light may have provided the driver of the following train with more warning No sand removal system fitted to 3801 No mechanism at the time for train to train or train to signalman communication communication with signal boxes was only possible by track side phones It is believed that the handbrakes on one of the carriages may have been applied as a stunt 2 Consequences EditAn interim ban was placed on the use of steam locomotives on the NSW railway system The ban was lifted 9 months later Operators were required to use one State Rail employee on each train Operators were required to carry insurance cover of 10 million The government agreed to underwrite any claims exceeding that amount See also EditGlenbrook rail accidentReferences Edit Fellows of Senate John Manning Ward AO Memorial Service http sydney edu au senate Ward memorial shtml Retrieved 17 February 2013 Pearce Kenn 1999 Australian railway disasters 2nd ed IPL Books ISBN 978 0 908876 09 9 1990 May 6 Cowan rail emergency Emergency Management NSW Archived from the original on 2 October 2013 Retrieved 15 September 2010 RAIL SAFETY ACT 1993 NEW SOUTH WALES Retrieved 15 September 2010 Retrieved from https en wikipedia org w index php title Cowan rail accident amp oldid 1158109075, wikipedia, wiki, book, books, library,

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