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Kegworth air disaster

British Midland Airways Flight 092, a Boeing 737-400, crashed onto the motorway embankment between the M1 motorway and A453 road near Kegworth, Leicestershire, England, while attempting to make an emergency landing at East Midlands Airport on 8 January 1989.[1]

British Midland Airways Flight 092
The scene of the disaster, with the runway that G-OBME failed to reach at the top of the picture
Accident
Date8 January 1989
SummaryFailure of one engine followed by erroneous shut-down of the operating engine, Stalled and crashed during emergency landing
SiteEast Midlands Airport, Kegworth, Leicestershire, England
52°49′55″N 1°17′57.5″W / 52.83194°N 1.299306°W / 52.83194; -1.299306
Aircraft
Aircraft typeBoeing 737-4Y0
OperatorBritish Midland
IATA flight No.BD092
ICAO flight No.BMA092
Call signMIDLAND 092
RegistrationG-OBME
Flight originLondon Heathrow Airport
DestinationBelfast International Airport
Occupants126
Passengers118
Crew8
Fatalities47
Injuries74
Survivors79 (71 passengers and all 8 crew) (initially 87)

The aircraft was on a scheduled flight from London Heathrow Airport to Belfast International Airport when a fan blade broke in the left engine, disrupting the air conditioning and filling the cabin with smoke. The pilots believed this indicated a fault in the right engine, since earlier models of the 737 ventilated the cabin from the right, and they were unaware that the 737-400 used a different system. The pilots mistakenly shut down the functioning engine. They selected full thrust from the malfunctioning one and this increased its fuel supply, causing it to catch fire. Of the 126 people aboard, 47 died and 74 sustained serious injuries. The inquiry attributed the blade fracture to metal fatigue, caused by heavy vibration in the newly upgraded engines, which had been tested only in the laboratory and not under representative flight conditions.

The accident was the first hull loss of a Boeing 737 Classic aircraft,[2] and the first fatal accident (and second fatal occurrence) involving a Boeing 737 Classic aircraft.[3]

Aircraft involved and crew edit

 
Sister aircraft of the accident aircraft, G-OBMF

Aircraft edit

The aircraft was a British Midland-operated Boeing 737-4Y0,[a] registration G-OBME,[4] on a scheduled flight from London Heathrow Airport to Belfast International Airport, Northern Ireland, having already flown from Heathrow to Belfast and back that day. The 737-400 was the newest design from Boeing, with the first unit entering service less than four months earlier, in September 1988. G-OBME itself had been in service for 85 days, since 15 October 1988, and had accumulated 521 airframe hours. The aircraft was powered by two CFM International CFM56 turbofan engines.[5][6][7]

Cockpit crew edit

The flight was crewed by 43-year-old Captain Kevin Hunt and 39-year-old First Officer David McClelland. Captain Hunt was a veteran British Midland pilot who had been with the airline since 1966 and had about 13,200 hours of flying experience. First Officer McClelland joined British Midland in 1988 and had accrued roughly 3,300 total flight hours. Between them, the pilots had close to 1,000 hours in the Boeing 737 cockpit (Hunt had 763 hours, and McClelland had 192 hours). However, only 76 of these were logged in Boeing 737-400 series aircraft (Hunt 23 hours and McClelland 53 hours).[8]

Accident edit

 
Photograph of the location of the disaster in May 2006

After taking off from Heathrow at 19:52,[b] Flight BD 092 was climbing through 28,300 feet (8,600 m) to reach its cruising altitude of 35,000 feet (11,000 m) when a blade detached from the fan of the port (left) engine. While the pilots did not know the source of the problem, a pounding noise was suddenly heard, accompanied by severe vibrations. In addition, smoke poured into the cabin through the ventilation system, and passengers became aware of the smell of burning.[9] Several passengers sitting near the rear of the plane noticed smoke and sparks coming from the left engine.[10] The flight was diverted to nearby East Midlands Airport[11] at the suggestion of British Midland Airways Operations.[12]

After the initial blade fracture, Captain Kevin Hunt had disengaged the plane's autopilot.[13] When Hunt asked First Officer David McClelland which engine was malfunctioning, McClelland replied: "It's the left.... It's the right one".[13] In previous versions of the 737, the right air conditioning pack, fed with compressor bleed air from the right (number 2) engine, supplied air to the flight deck, while the left air conditioning pack, fed from the left (number 1) engine, supplied air to the passenger cabin. On the 737-400, this division of air is blurred; the left pack feeds the flight deck, but also feeds the aft passenger cabin, while the right feeds the forward passenger cabin. The pilots had been used to the older version of the aircraft and did not realise that this aircraft (which had been flown by British Midland for only 520 hours over a two-month period) was different. The captain later claimed that his perception of smoke as coming forward from the passenger cabin led them to assume the fault was in the right engine.[14] The pilots throttled back the working right engine instead of the malfunctioning left engine.[14] They had no way of visually checking the engines from the cockpit, and the cabin crew — who did not hear the captain refer to the right hand engine in his cabin address — did not inform them that smoke and flames had been seen from the left engine.[15]

When the pilots shut down the right engine, they could no longer smell the smoke, which led them to believe that they had correctly dealt with the problem. As it turned out, this was a coincidence; when the autothrottle was disengaged prior to shutting down the right engine, the fuel flow to both engines was reduced, and the excess fuel, which had been igniting in the left engine exhaust, disappeared; therefore, the ongoing damage was reduced, the smell of smoke ceased, and the vibration reduced, although it would still have been visible on cockpit instruments.[16]

 
Wreckage of G-OBME

During the final approach to the East Midlands Airport, the pilots selected increased thrust from the operating, damaged engine. This led to an engine fire that caused the engine to cease operating entirely. The ground proximity warning system activated, sounding several "glideslope" warnings. The pilots attempted to restart the right engine by windmilling, but the aircraft was by now flying at 185 km/h (100 kn; 115 mph), too slow for a restart. At 20:24:33, Captain Hunt broadcast to the passengers via the aircraft's public-address system: "Prepare for crash landing," instructing passengers to take the brace position. The stick shaker then activated. Just before crossing the M1 motorway at 20:24:43, the tail and main landing gear struck the ground and the aircraft bounced back into the air and over the motorway, knocking down trees and a lamp post before crashing on the far embankment around 475 m (519 yd) short of the active runway's paved surface and about 630 m (689 yd) from its threshold. The aircraft broke into three sections.[17] This was adjacent to the motorway; remarkably, no vehicles were travelling on that part of the M1 at the moment of the crash.[18]

Casualties edit

Of the 118 passengers on board, 39 were killed outright in the crash and eight died later of their injuries, for a total of 47 fatalities. All eight crew members survived the accident. Of the 79 survivors, 74 suffered serious injuries and five suffered minor injuries. In addition, five firefighters also suffered minor injuries during the rescue operation.[19] No one on the motorway was injured, and all vehicles in the vicinity of the disaster were undamaged. The first person to arrive at the scene to render aid was a motorist, Graham Pearson.[20] A former Royal Marine, he helped passengers for over three hours and subsequently received damages for post-traumatic stress disorder.[20] Aid was also given by a troop of eight SAS soldiers, four of whom were regimentally qualified paramedics. Their truck had been on the motorway when the crash occurred.[21]

Causes edit

The investigation established that the wiring associated with the fire warning lights was not cross-wired (left/right), i.e. it was properly connected.[22]

Shutting down of wrong engine edit

Captain Hunt believed the right engine was malfunctioning due to the smell of smoke in the cabin because in previous Boeing 737 variants bleed air for cabin air conditioning was taken from the right engine. Starting with the Boeing 737-400 variant, Boeing had redesigned the system to use bleed air from both engines.[citation needed] Several cabin staff and passengers noticed that the left engine had a stream of unburnt fuel igniting in the jet exhaust, but this information was not passed to the pilots because cabin staff assumed they were aware that the left engine was malfunctioning.[23]

The smell of smoke disappeared when the autothrottle was disengaged and the right engine shut down due to reduction of fuel to the damaged left engine as it reverted to manual throttle.[16] In the event of a malfunction, pilots were trained to check all meters and review all decisions, and Captain Hunt proceeded to do so. Whilst he was conducting the review, however, he was interrupted by a transmission from East Midlands Airport informing him he could descend further to 12,000 feet (3,700 m) in preparation for the diverted landing. He did not resume the review after the transmission ended, and instead commenced descent.[citation needed]

The dials on the two vibration gauges (one for each engine) were smaller than on the previous versions of the 737 in which the pilots had the majority of their experience and the LED needle went around the outside of the dial as opposed to the inside.[24] The pilots had received no simulator training on the new model, as no simulator for the 737-400 existed in the UK at that time. At the time, vibration indicators were known for being unreliable[25] (and normally ignored by pilots), but unknown to the pilots, this was one of the first aircraft to have a very accurate vibration readout.[10]

Engine malfunction edit

Analysis of the engine from the crash determined that the fan blades (LP stage 1 compressor) of the uprated CFM International CFM56 engine used on the 737-400 were subject to abnormal amounts of vibration when operating at high power settings above 10,000 feet (3,000 m).[26] As it was an upgrade to an existing engine, in-flight testing was not mandatory, and the engine had only been tested in the laboratory. Upon this discovery, the remaining 99 Boeing 737-400s then in service were grounded and the engines modified. Following the crash, testing all newly designed and significantly redesigned turbofan engines under representative flight conditions is now mandatory.

This unnoticed vibration created excessive metal fatigue in the fan blades, and on G-OBME, this caused one of the fan blades to break off. This damaged the engine terminally and also upset its delicate balance, causing a reduction in power and an increase in vibration. The autothrottle attempted to compensate for this by increasing the fuel flow to the engine. The damaged engine was unable to burn all the additional fuel, with much of it igniting in the exhaust flow, creating a large trail of flame behind the engine.

Aftermath edit

 
Memorial scroll in St Anne's Cathedral, Belfast

The official report into the disaster made 31 safety recommendations.[27] Evaluation of the injuries sustained led to considerable improvements in aircraft safety and emergency instructions for passengers.[10] These were derived from a research programme funded by the CAA and carried out by teams from the University of Nottingham and Hawtal Whiting Structures (an engineering consultancy company). The study between medical staff and engineers used analytical "occupant kinematics" techniques to assess the effectiveness of the brace position.[28] A new notice to operators revising the brace position was issued in October 1993.

The research into this accident led to the formation on 21 November 2016 of the International Board for Research into Aircraft Crash Events, which is a joint co-operation between experts in the field for the purpose of producing an internationally agreed-upon, evidence-based set of impact bracing positions for passengers and (eventually) cabin crew members in a variety of seating configurations. These will be submitted to the International Civil Aviation Organization through its Cabin Safety Group.

 
Memorial garden at Kegworth cemetery

A memorial was built to "those who died, those who were injured and those who took part in the rescue operation", in the village cemetery in nearby Kegworth, together with a garden made using soil from the crash site.[29]

Captain Hunt and First Officer McClelland, both seriously injured in the crash, were dismissed following the criticisms of their actions in the Air Accidents Investigation Branch report.[30] Hunt suffered injuries to his spine and legs in the crash. In April 1991, he told a BBC documentary: "We were the easy option—the cheap option if you wish. We made a mistake — we both made mistakes — but the question we would like answered is why we made those mistakes."[31] BM later paid McClelland an out-of-court settlement for unfair dismissal.[10]

Alan Webb, the chief fire officer at East Midlands Airport, was made an MBE in the 1990 New Year Honours list for the co-ordination of his team in the rescue efforts that followed the crash.[32] Graham Pearson, a passing motorist who assisted Kegworth survivors at the crash site for three hours, sued the airline for post-traumatic stress disorder and was awarded £57,000 in damages in 1998 (equivalent to £85,200 in 2019).[20]

Media edit

The crash was featured in a 1991 documentary of Taking Liberties named "Fatal Error". ITV aired a documentary in 1999 of the Kegworth crash. Flight 092 was also featured in an episode of Seconds From Disaster, called "Motorway Plane Crash".

It was also featured in the 2011 Discovery Channel documentary Aircrash Confidential.[33]

In 2015, the incident was featured in the episode "Choosing Sides" or "M1 Plane Crash" of the documentary television series Mayday or Air Crash Investigation as it is known in the UK.[34]

See also edit

Notes edit

  1. ^ The aircraft was a Boeing 737-400 model; Boeing assigns a unique customer code for each company that buys one of its aircraft, which is applied as a suffix to the model number at the time the aircraft is built. The code "Y0" was assigned to the leasing company Guinness Peat Aviation, from whom British Midland leased the aircraft.
  2. ^ McClelland was the pilot flying until the engine failure, after which Captain Hunt took control.[8]

References edit

References
  1. ^ Ranter, Harro. "ASN Aircraft accident Boeing 737-4Y0 G-OBME Kegworth". aviation-safety.net. Aviation Safety Network. Retrieved 12 July 2019.
  2. ^ Ranter, Harro. "Accident list: Boeing 737". aviation-safety.net. Aviation Safety Network. Retrieved 12 September 2021.
  3. ^ Ranter, Harro. "Accident list: Boeing 737". aviation-safety.net. Aviation Safety Network. Retrieved 12 September 2021.
  4. ^ "G-INFO Database". Civil Aviation Authority.
  5. ^ Trimble 1990, p. 11–22.
  6. ^ "G-OBME British Midland Boeing 737-400". www.planespotters.net. Retrieved 31 March 2020.
  7. ^ "British Midland Airways G-OBME (Boeing 737 – MSN 23867)". www.airfleets.net. Airfleets aviation. Retrieved 31 March 2020.
  8. ^ a b Trimble 1990, p. 8–9.
  9. ^ Trimble 1990, p. 1.
  10. ^ a b c d Truslove, Ben (8 January 2014). "Kegworth air disaster: Plane crash survivors' stories". BBC News. BBC Online. Archived from the original on 8 January 2014. Retrieved 8 January 2014. – The content about the safety improvements is from the sidebar "The legacy of Kegworth".
  11. ^ Trimble 1990, p. 103.
  12. ^ Trimble 1990, p. 4.
  13. ^ a b Trimble 1990, p. 3.
  14. ^ a b Trimble 1990, p. 98.
  15. ^ Trimble 1990, p. 5.
  16. ^ a b Trimble 1990, p. 99.
  17. ^ Trimble 1990, p. 7–8.
  18. ^ "Why did British Midland plane crash on the M1 near Kegworth?". ITV News. ITV. ITV Report. 8 January 2014. Retrieved 13 January 2017.
  19. ^ Trimble 1990, p. 7.
  20. ^ a b c "UK, Air crash hero wins damages". BBC News. BBC. 10 February 1998. Retrieved 16 May 2011.
  21. ^ Ramsey, Jack (1996). SAS: The soldiers story. London: Pan. pp. 59–64. ISBN 0330347500.
  22. ^ Trimble 1990, p. 125.
  23. ^ Trimble 1990, p. 106.
  24. ^ Trimble 1990, p. 69.
  25. ^ Trimble 1990, p. 69–70.
  26. ^ Trimble 1990, p. 118–120.
  27. ^ Trimble 1990, p. 149–152.
  28. ^ Scientific and Technical Aerospace Reports. NASA, Office of Scientific and Technical Information. 1993. p. 1423.
  29. ^ "Kegworth Village, Kegworth Air Disaster 1989". www.kegworthvillage.com. Retrieved 16 August 2021.
  30. ^ Brookes, Andrew (1994). Disaster in the air. p. 135. ISBN 0-7110-2037-X.
  31. ^ This is Nottingham (8 January 2009), Kegworth: Sacked pilots claim they were 'scapegoats', Nottinghampost.com, retrieved 8 January 2014
  32. ^ "No. 519981". The London Gazette (Supplement). 29 December 1989. p. 15.
  33. ^ . Yourdiscovery.com. 24 February 2011. Archived from the original on 12 May 2011. Retrieved 16 May 2011.
  34. ^ Mayday - Air Crash Investigation (S01-S22), retrieved 16 February 2024
Bibliography
  • Macarthur Job, Air Disaster Volume 2: Aerospace Publications Pty Ltd, 1996, ISBN 1-875671-19-6, p. 173–185
  • David Owen, Air Accident Investigation: Patrick Stephens Limited, 2001, ISBN 0-7509-4495-1. (The Kegworth air disaster is given a detailed mention in Chapter 9, "Pressing the Wrong Button")
  • HW Structures, CAA Paper 90012 Occupant modelling in aircraft crash conditions: Civil Aviation Authority, 1990, ISBN 0-86039-445-X.
  • Hawtal Whiting Technology Group, CAA Paper 95004 A study of aircraft passenger brace positions for impact: Civil Aviation Authority, 1995, ISBN 0-86039-620-7
  • Trimble, E J (1990), Report No: 4/1990. Report on the accident to Boeing 737-400, G-OBME, near Kegworth, Leicestershire on 8 January 1989, Air Accidents Investigation Branch
    • Report file ()
    • Appendices ()

External links edit

  • BBC 10th anniversary page about the crash
  • BBC 'On This Day' page about the crash
  • Pre-crash and crash pictures of the aircraft from Airliners.net
  • Field, James (8 January 2019). . Airways International. Archived from the original on 8 January 2019. Retrieved 8 January 2019.
  • Accident description at the Aviation Safety Network

kegworth, disaster, this, article, needs, additional, citations, verification, please, help, improve, this, article, adding, citations, reliable, sources, unsourced, material, challenged, removed, find, sources, news, newspapers, books, scholar, jstor, october. This article needs additional citations for verification Please help improve this article by adding citations to reliable sources Unsourced material may be challenged and removed Find sources Kegworth air disaster news newspapers books scholar JSTOR October 2010 Learn how and when to remove this message British Midland Airways Flight 092 a Boeing 737 400 crashed onto the motorway embankment between the M1 motorway and A453 road near Kegworth Leicestershire England while attempting to make an emergency landing at East Midlands Airport on 8 January 1989 1 British Midland Airways Flight 092The scene of the disaster with the runway that G OBME failed to reach at the top of the pictureAccidentDate8 January 1989SummaryFailure of one engine followed by erroneous shut down of the operating engine Stalled and crashed during emergency landingSiteEast Midlands Airport Kegworth Leicestershire England 52 49 55 N 1 17 57 5 W 52 83194 N 1 299306 W 52 83194 1 299306AircraftAircraft typeBoeing 737 4Y0OperatorBritish MidlandIATA flight No BD092ICAO flight No BMA092Call signMIDLAND 092RegistrationG OBMEFlight originLondon Heathrow AirportDestinationBelfast International AirportOccupants126Passengers118Crew8Fatalities47Injuries74Survivors79 71 passengers and all 8 crew initially 87 The aircraft was on a scheduled flight from London Heathrow Airport to Belfast International Airport when a fan blade broke in the left engine disrupting the air conditioning and filling the cabin with smoke The pilots believed this indicated a fault in the right engine since earlier models of the 737 ventilated the cabin from the right and they were unaware that the 737 400 used a different system The pilots mistakenly shut down the functioning engine They selected full thrust from the malfunctioning one and this increased its fuel supply causing it to catch fire Of the 126 people aboard 47 died and 74 sustained serious injuries The inquiry attributed the blade fracture to metal fatigue caused by heavy vibration in the newly upgraded engines which had been tested only in the laboratory and not under representative flight conditions The accident was the first hull loss of a Boeing 737 Classic aircraft 2 and the first fatal accident and second fatal occurrence involving a Boeing 737 Classic aircraft 3 Contents 1 Aircraft involved and crew 1 1 Aircraft 1 2 Cockpit crew 2 Accident 3 Casualties 4 Causes 4 1 Shutting down of wrong engine 4 2 Engine malfunction 5 Aftermath 6 Media 7 See also 8 Notes 9 References 10 External linksAircraft involved and crew edit nbsp Sister aircraft of the accident aircraft G OBMF Aircraft edit The aircraft was a British Midland operated Boeing 737 4Y0 a registration G OBME 4 on a scheduled flight from London Heathrow Airport to Belfast International Airport Northern Ireland having already flown from Heathrow to Belfast and back that day The 737 400 was the newest design from Boeing with the first unit entering service less than four months earlier in September 1988 G OBME itself had been in service for 85 days since 15 October 1988 and had accumulated 521 airframe hours The aircraft was powered by two CFM International CFM56 turbofan engines 5 6 7 Cockpit crew edit The flight was crewed by 43 year old Captain Kevin Hunt and 39 year old First Officer David McClelland Captain Hunt was a veteran British Midland pilot who had been with the airline since 1966 and had about 13 200 hours of flying experience First Officer McClelland joined British Midland in 1988 and had accrued roughly 3 300 total flight hours Between them the pilots had close to 1 000 hours in the Boeing 737 cockpit Hunt had 763 hours and McClelland had 192 hours However only 76 of these were logged in Boeing 737 400 series aircraft Hunt 23 hours and McClelland 53 hours 8 Accident edit nbsp Photograph of the location of the disaster in May 2006 After taking off from Heathrow at 19 52 b Flight BD 092 was climbing through 28 300 feet 8 600 m to reach its cruising altitude of 35 000 feet 11 000 m when a blade detached from the fan of the port left engine While the pilots did not know the source of the problem a pounding noise was suddenly heard accompanied by severe vibrations In addition smoke poured into the cabin through the ventilation system and passengers became aware of the smell of burning 9 Several passengers sitting near the rear of the plane noticed smoke and sparks coming from the left engine 10 The flight was diverted to nearby East Midlands Airport 11 at the suggestion of British Midland Airways Operations 12 After the initial blade fracture Captain Kevin Hunt had disengaged the plane s autopilot 13 When Hunt asked First Officer David McClelland which engine was malfunctioning McClelland replied It s the left It s the right one 13 In previous versions of the 737 the right air conditioning pack fed with compressor bleed air from the right number 2 engine supplied air to the flight deck while the left air conditioning pack fed from the left number 1 engine supplied air to the passenger cabin On the 737 400 this division of air is blurred the left pack feeds the flight deck but also feeds the aft passenger cabin while the right feeds the forward passenger cabin The pilots had been used to the older version of the aircraft and did not realise that this aircraft which had been flown by British Midland for only 520 hours over a two month period was different The captain later claimed that his perception of smoke as coming forward from the passenger cabin led them to assume the fault was in the right engine 14 The pilots throttled back the working right engine instead of the malfunctioning left engine 14 They had no way of visually checking the engines from the cockpit and the cabin crew who did not hear the captain refer to the right hand engine in his cabin address did not inform them that smoke and flames had been seen from the left engine 15 When the pilots shut down the right engine they could no longer smell the smoke which led them to believe that they had correctly dealt with the problem As it turned out this was a coincidence when the autothrottle was disengaged prior to shutting down the right engine the fuel flow to both engines was reduced and the excess fuel which had been igniting in the left engine exhaust disappeared therefore the ongoing damage was reduced the smell of smoke ceased and the vibration reduced although it would still have been visible on cockpit instruments 16 nbsp Wreckage of G OBME During the final approach to the East Midlands Airport the pilots selected increased thrust from the operating damaged engine This led to an engine fire that caused the engine to cease operating entirely The ground proximity warning system activated sounding several glideslope warnings The pilots attempted to restart the right engine by windmilling but the aircraft was by now flying at 185 km h 100 kn 115 mph too slow for a restart At 20 24 33 Captain Hunt broadcast to the passengers via the aircraft s public address system Prepare for crash landing instructing passengers to take the brace position The stick shaker then activated Just before crossing the M1 motorway at 20 24 43 the tail and main landing gear struck the ground and the aircraft bounced back into the air and over the motorway knocking down trees and a lamp post before crashing on the far embankment around 475 m 519 yd short of the active runway s paved surface and about 630 m 689 yd from its threshold The aircraft broke into three sections 17 This was adjacent to the motorway remarkably no vehicles were travelling on that part of the M1 at the moment of the crash 18 Casualties editOf the 118 passengers on board 39 were killed outright in the crash and eight died later of their injuries for a total of 47 fatalities All eight crew members survived the accident Of the 79 survivors 74 suffered serious injuries and five suffered minor injuries In addition five firefighters also suffered minor injuries during the rescue operation 19 No one on the motorway was injured and all vehicles in the vicinity of the disaster were undamaged The first person to arrive at the scene to render aid was a motorist Graham Pearson 20 A former Royal Marine he helped passengers for over three hours and subsequently received damages for post traumatic stress disorder 20 Aid was also given by a troop of eight SAS soldiers four of whom were regimentally qualified paramedics Their truck had been on the motorway when the crash occurred 21 Causes editThe investigation established that the wiring associated with the fire warning lights was not cross wired left right i e it was properly connected 22 Shutting down of wrong engine edit Captain Hunt believed the right engine was malfunctioning due to the smell of smoke in the cabin because in previous Boeing 737 variants bleed air for cabin air conditioning was taken from the right engine Starting with the Boeing 737 400 variant Boeing had redesigned the system to use bleed air from both engines citation needed Several cabin staff and passengers noticed that the left engine had a stream of unburnt fuel igniting in the jet exhaust but this information was not passed to the pilots because cabin staff assumed they were aware that the left engine was malfunctioning 23 The smell of smoke disappeared when the autothrottle was disengaged and the right engine shut down due to reduction of fuel to the damaged left engine as it reverted to manual throttle 16 In the event of a malfunction pilots were trained to check all meters and review all decisions and Captain Hunt proceeded to do so Whilst he was conducting the review however he was interrupted by a transmission from East Midlands Airport informing him he could descend further to 12 000 feet 3 700 m in preparation for the diverted landing He did not resume the review after the transmission ended and instead commenced descent citation needed The dials on the two vibration gauges one for each engine were smaller than on the previous versions of the 737 in which the pilots had the majority of their experience and the LED needle went around the outside of the dial as opposed to the inside 24 The pilots had received no simulator training on the new model as no simulator for the 737 400 existed in the UK at that time At the time vibration indicators were known for being unreliable 25 and normally ignored by pilots but unknown to the pilots this was one of the first aircraft to have a very accurate vibration readout 10 Engine malfunction edit Analysis of the engine from the crash determined that the fan blades LP stage 1 compressor of the uprated CFM International CFM56 engine used on the 737 400 were subject to abnormal amounts of vibration when operating at high power settings above 10 000 feet 3 000 m 26 As it was an upgrade to an existing engine in flight testing was not mandatory and the engine had only been tested in the laboratory Upon this discovery the remaining 99 Boeing 737 400s then in service were grounded and the engines modified Following the crash testing all newly designed and significantly redesigned turbofan engines under representative flight conditions is now mandatory This unnoticed vibration created excessive metal fatigue in the fan blades and on G OBME this caused one of the fan blades to break off This damaged the engine terminally and also upset its delicate balance causing a reduction in power and an increase in vibration The autothrottle attempted to compensate for this by increasing the fuel flow to the engine The damaged engine was unable to burn all the additional fuel with much of it igniting in the exhaust flow creating a large trail of flame behind the engine Aftermath edit nbsp Memorial scroll in St Anne s Cathedral Belfast The official report into the disaster made 31 safety recommendations 27 Evaluation of the injuries sustained led to considerable improvements in aircraft safety and emergency instructions for passengers 10 These were derived from a research programme funded by the CAA and carried out by teams from the University of Nottingham and Hawtal Whiting Structures an engineering consultancy company The study between medical staff and engineers used analytical occupant kinematics techniques to assess the effectiveness of the brace position 28 A new notice to operators revising the brace position was issued in October 1993 The research into this accident led to the formation on 21 November 2016 of the International Board for Research into Aircraft Crash Events which is a joint co operation between experts in the field for the purpose of producing an internationally agreed upon evidence based set of impact bracing positions for passengers and eventually cabin crew members in a variety of seating configurations These will be submitted to the International Civil Aviation Organization through its Cabin Safety Group nbsp Memorial garden at Kegworth cemetery A memorial was built to those who died those who were injured and those who took part in the rescue operation in the village cemetery in nearby Kegworth together with a garden made using soil from the crash site 29 Captain Hunt and First Officer McClelland both seriously injured in the crash were dismissed following the criticisms of their actions in the Air Accidents Investigation Branch report 30 Hunt suffered injuries to his spine and legs in the crash In April 1991 he told a BBC documentary We were the easy option the cheap option if you wish We made a mistake we both made mistakes but the question we would like answered is why we made those mistakes 31 BM later paid McClelland an out of court settlement for unfair dismissal 10 Alan Webb the chief fire officer at East Midlands Airport was made an MBE in the 1990 New Year Honours list for the co ordination of his team in the rescue efforts that followed the crash 32 Graham Pearson a passing motorist who assisted Kegworth survivors at the crash site for three hours sued the airline for post traumatic stress disorder and was awarded 57 000 in damages in 1998 equivalent to 85 200 in 2019 20 Media editThe crash was featured in a 1991 documentary ofTaking Liberties named Fatal Error ITV aired a documentary in 1999 of the Kegworth crash Flight 092 was also featured in an episode of Seconds From Disaster called Motorway Plane Crash It was also featured in the 2011 Discovery Channel documentary Aircrash Confidential 33 In 2015 the incident was featured in the episode Choosing Sides or M1 Plane Crash of the documentary television series Mayday or Air Crash Investigation as it is known in the UK 34 See also editTransAsia Airways Flight 235 SA Airlink Flight 8911 Transair Flight 810 and Azerbaijan Airlines Flight 56 other cases of misidentification of a failing engine List of accidents and incidents involving commercial aircraftNotes edit The aircraft was a Boeing 737 400 model Boeing assigns a unique customer code for each company that buys one of its aircraft which is applied as a suffix to the model number at the time the aircraft is built The code Y0 was assigned to the leasing company Guinness Peat Aviation from whom British Midland leased the aircraft McClelland was the pilot flying until the engine failure after which Captain Hunt took control 8 References editReferences Ranter Harro ASN Aircraft accident Boeing 737 4Y0 G OBME Kegworth aviation safety net Aviation Safety Network Retrieved 12 July 2019 Ranter Harro Accident list Boeing 737 aviation safety net Aviation Safety Network Retrieved 12 September 2021 Ranter Harro Accident list Boeing 737 aviation safety net Aviation Safety Network Retrieved 12 September 2021 G INFO Database Civil Aviation Authority Trimble 1990 p 11 22 G OBME British Midland Boeing 737 400 www planespotters net Retrieved 31 March 2020 British Midland Airways G OBME Boeing 737 MSN 23867 www airfleets net Airfleets aviation Retrieved 31 March 2020 a b Trimble 1990 p 8 9 Trimble 1990 p 1 a b c d Truslove Ben 8 January 2014 Kegworth air disaster Plane crash survivors stories BBC News BBC Online Archived from the original on 8 January 2014 Retrieved 8 January 2014 The content about the safety improvements is from the sidebar The legacy of Kegworth Trimble 1990 p 103 Trimble 1990 p 4 a b Trimble 1990 p 3 a b Trimble 1990 p 98 Trimble 1990 p 5 a b Trimble 1990 p 99 Trimble 1990 p 7 8 Why did British Midland plane crash on the M1 near Kegworth ITV News ITV ITV Report 8 January 2014 Retrieved 13 January 2017 Trimble 1990 p 7 a b c UK Air crash hero wins damages BBC News BBC 10 February 1998 Retrieved 16 May 2011 Ramsey Jack 1996 SAS The soldiers story London Pan pp 59 64 ISBN 0330347500 Trimble 1990 p 125 Trimble 1990 p 106 Trimble 1990 p 69 Trimble 1990 p 69 70 Trimble 1990 p 118 120 Trimble 1990 p 149 152 Scientific and Technical Aerospace Reports NASA Office of Scientific and Technical Information 1993 p 1423 Kegworth Village Kegworth Air Disaster 1989 www kegworthvillage com Retrieved 16 August 2021 Brookes Andrew 1994 Disaster in the air p 135 ISBN 0 7110 2037 X This is Nottingham 8 January 2009 Kegworth Sacked pilots claim they were scapegoats Nottinghampost com retrieved 8 January 2014 No 519981 The London Gazette Supplement 29 December 1989 p 15 Aircrash Confidential Lethal Malfunctions Videos at Yourdiscovery com 24 February 2011 Archived from the original on 12 May 2011 Retrieved 16 May 2011 Mayday Air Crash Investigation S01 S22 retrieved 16 February 2024 Bibliography Macarthur Job Air Disaster Volume 2 Aerospace Publications Pty Ltd 1996 ISBN 1 875671 19 6 p 173 185 David Owen Air Accident Investigation Patrick Stephens Limited 2001 ISBN 0 7509 4495 1 The Kegworth air disaster is given a detailed mention in Chapter 9 Pressing the Wrong Button HW Structures CAA Paper 90012 Occupant modelling in aircraft crash conditions Civil Aviation Authority 1990 ISBN 0 86039 445 X Hawtal Whiting Technology Group CAA Paper 95004 A study of aircraft passenger brace positions for impact Civil Aviation Authority 1995 ISBN 0 86039 620 7 Trimble E J 1990 Report No 4 1990 Report on the accident to Boeing 737 400 G OBME near Kegworth Leicestershire on 8 January 1989 Air Accidents Investigation Branch Report file G OBME pdf Archive Appendices G OBME Append pdf Archive External links editBBC 10th anniversary page about the crash BBC On This Day page about the crash Pre crash and crash pictures of the aircraft from Airliners net Field James 8 January 2019 Op Ed Learning From The Kegworth Air Disaster 30 Years On Airways International Archived from the original on 8 January 2019 Retrieved 8 January 2019 Accident description at the Aviation Safety Network Portals nbsp Aviation nbsp England nbsp 1980s Retrieved from https en wikipedia org w index php title Kegworth air disaster amp oldid 1223581986, wikipedia, wiki, book, books, library,

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